HEALTH CARE DISTRICT OF PALM BEACH COUNTY

Part 135 operator · designator HC7A

Data confidence: All records on this page are linked by a shared certificate number or aircraft registration (N-number).

Also recorded as: HEALTH CARE DISTRICT OF PALM BEACH COUNTY, HEALTH CARE DISTRICT-TRAUMA HAWK

Accident & enforcement record

Events that happened, regardless of the operator's own reporting. Each links to its public source.

NTSB accidents & incidents

No NTSB accidents or incidents linked to this operator.

FAA enforcement actions

FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.

Maintenance disclosure history

Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.

4 reports on file.

B · 2018-01-22 Matched by certificate designator
N911PB · ATA 2150

AIRCRAFT WAS IN CRUISE FLIGHT, THE AIR CONDITIONING WAS TURNED ON, A BURNING SMELL WAS SOON NOTICED, THE A/C WAS THEN TURNED OFF, THE SMELL IMMEDIATELY DISSIPATED. THE AIRCRAFT RETURNED TO BASE. TECHNICIAN INSPECTED THE A/C SYSTEM TO INCLUDE THE EVAP BLOWER, IT WAS NOTICED THE EVAP MOTOR DID NOT OPERATE IN THE LOW MODE. EVAP MOTOR WAS REMOVED AND INSPECTED. THERE ARE TWO RESISTORS MOUNTED INSIDE THE MOTOR CAGE ASSY, ONE FOR EACH HIGH/LOW SETTING. THERE APPEARED TO BE NO VISUAL INDICATIONS OF ARCING OR OTHERWISE, THERE WAS A SLIGHT BURNT SMELL IN THAT LOCATION. THE EVAP BLOWER ASSY WAS REPLACED WITH A NEW UNIT, ALL OPERATIONAL TESTS WERE NORMAL WITH NO DEFECTS NOTED. AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR HC7A201801230001 · FAA SDRS
N · 2016-06-12 Matched by certificate designator
N911PB · ATA 2697

AFTER AIRCRAFT LANDED AND DURING THROTTLE REDUCTION TO IDLE, THE NR 1 ENGINE FLAME DETECTOR FLICKERED ON AND OFF TWICE, APPROXIMATELY 1 SECOND EACH TIME. ACFT WAS SHUTDOWN, AND MAINTENANCE VISUALLY INSPECTED THE ENGINE AREA, NO EVIDENCE OF A FIRE WAS NOTED. A COCKPIT TEST OF THE FIRE DETECTION SYS WAS COMPLETED WITH NO DEFECTS NOTED. THE FLAME DETECTOR WAS REMOVED, VISUALLY INSPECTED, THE CONNECTOR PLUG AND DETECTOR WERE CLEANED. THE DETECTOR WAS SWAPPED WITH THE NR 2 SIDE TO FURTHER HELP IN TROUBLESHOOTING. A COMPLETE FIRE DETECTION OPS TEST USING THE SIMULATED FIRE TEST BOX WAS CONDUCTED WITH NO DEFECTS NOTED. THE ACFT WAS GROUND RUN AND FLOWN TWICE ALSO WITH NO DEFECTS NOTED. ACFT WAS RETURNED TO SERVICE.

Source: SDR HC7A201606120001 · FAA SDRS
D · 2012-04-19 Matched by certificate designator
N276TH · ATA 5220

SHORTLY AFTER LIFT OFF, HATCH ASSY SEPARATED FROM ACFT. RETURNED TO AIRPORT AND LANDED WITHOUT INCIDENT. FOUND LATCH PARTS; PIVOT, SPRING, AND ROD WERE ALL DISCONNECTED FROM CLEVIS AND LOCK NUT MISSING. FINDINGS INDICATE THE ROD VIBRATED LOOSE AND THE ASSY CAME APART.

Source: SDR HC7A2012F00078 · FAA SDRS
O · 2011-04-02 Matched by certificate designator
N276TH · ATA 5302

DURING ROUTINE INSPECTION, THE UPPER LEFT STATION 300 TAIBOOM FITTING WAS FOUND TO BE CRACKED. THE CRACK APPEARED TO START AT THE BOLT HOLE AND EXTEND TO LOWER EDGE. THE FITTING WAS REPLACED IAW SIKORSKY STRUCTURAL REPAIR MANUAL AND THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR HC7A20110402001 · FAA SDRS

Linked aircraft

No aircraft currently linked.