SHIER AVIATION CORP

Part 135 operator · designator IVSA

Data confidence: All records on this page are linked by a shared certificate number or aircraft registration (N-number).

Also recorded as: CORPORATE HELICOPTERS, SHIER AVIATION CORP, Shier Aviation Corp

Accident & enforcement record

Events that happened, regardless of the operator's own reporting. Each links to its public source.

NTSB accidents & incidents

No NTSB accidents or incidents linked to this operator.

FAA enforcement actions

FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.

Maintenance disclosure history

Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.

25 reports on file.

K B · 2014-07-14 Matched by certificate designator
N491SA · ATA 8530

BAFFLING THAT SEPARATES THE OIL COOLER AND THE NR 2 CYLINDER, CRACKED AND SEPARATED. IT CAME TO REST ON THE STARTER POSITIVE TERMINAL AND NR 2 CYLINDER ROCKER BOX OIL RETURN LINE, PN 72703. WHEN THE STARTER WAS ENGAGED THE ELECTRICAL CURRENT ARCED THROUGH THE SHEET METAL BAFFLE TO THE OIL RETURN LINE SEVERING THE ALUMINUM TUBING. LOSS OF ENGINE OIL PRESSURE OCCURRED DURING START ACCOMPANIED BY SMOKE. OIL SPILLED TO THE GROUND BELOW THE ACFT.

Source: SDR FAA2014071400132 · FAA SDRS
O · 2002-05-07 Matched by certificate designator
NHP145 · ATA 6310

CLUTCH ACTUATOR MOTOR FAILED. (4TH TIME)

Source: SDR IVSA078654 · FAA SDRS
J · 2002-04-09 Matched by certificate designator
N7101J · ATA 6310

BELTS WERE REPLACED DURING 100HR INSPECTION AFTER 693.3 HOURS TSI. FAN WHEEL WAS BALANCED AND RUNUP WAS NORMAL. FIRST FLIGHT OF APPROXIMATELY 2 HOURS WAS UNEVENTFUL. DURING SECOND FLIGHT PILOT REPORTED CLUTCH LIGHT FLICKERED ON AND OFF SEVERAL TIMES. ON INSPECTION AFTER PRECAUTIONARY LANDING, BELTS WERE FOUND STRETCHED TO THE POINT THAT OVER LIMIT SWITCH DEACTIVATED THE SYSTEM. SYSTEM INSPECTED WITH NO FAULTS FOUND OTHER THAN BELT STRETCH BEYOND LIMITS. NEW BELTS WERE INSTALLED AND ADJUSTED. FAN WHEEL BALANCE CHECKED.

Source: SDR IVSA078430 · FAA SDRS
O · 2002-01-23 Matched by certificate designator
NHP145 · ATA 7600

GOVERNOR MOTOR RUNS SLOWLY, TAKING 10-12 SECONDS TO BRING RPM UP TO FLIGHT RPM REPLACEMENT MOTOR INSTALLED, DEFECTIVE UNIT RETURNED TO ROBINSON FOR WARRANTY EXCHANGE OR REPAIR.

Source: SDR IVSA077688 · FAA SDRS
O · 2001-12-12 Matched by certificate designator
N7186Z · ATA 6300

PAINT ON FAN WHEEL LOOSE AND FLAKING OFF DUE TO POOR ADHESION, PROBABLY CAUSED BY IMPROPER PREPARATION, ALLOWING PREMATURE CORROSION.

Source: SDR IVSA077371 · FAA SDRS
O · 2001-10-03 Matched by certificate designator
N335FP · ATA 6210

BLADE REMOVED FOR REPAIR OF LEADING EDGE ABRASION STRIP CRACKS. CUSTOMER REQUESTED EXCHANGE BLADE IN ORDER TO RESUME FLIGHTS. EXCHANGE BLADE INSTALLED, REPAIRABLE BLADE RETURNED TO AEC

Source: SDR IVSA076105 · FAA SDRS
O · 2001-09-24 Matched by certificate designator
N7189C · ATA 6320

CLUTCH ACTUATOR MOTOR FAILED FOR THE 2ND TIME. REPLACEMENT MOTOR INSTALLED. FURTHER TOUBLESHOOTING REVEALED SHEAVE ALIGNMENT OUT OF LIMITS CAUSING INFLIGHT ILLUMINATION OF CLUTCH LIGHT. ALIGNMENT CORRECTED AND FLIGHTS CONTINUED NORMALLY. BAD MOTOR RETURNED FOR WARRANTY CREDIT.

Source: SDR IVSA075920 · FAA SDRS
O · 2001-08-31 Matched by certificate designator
NUNK · ATA 6310

MOTOR FAILED TO OPERATE WHEN CALLED ON TO ENGAGE M/R DRIVE BELTS. WOULD NOT OPERATE IN EITHER DIRECTION. MOTOR REPLACED, DEFECTIVE MOTOR RETURNED TOROBINSON FOR WARRANTY CREDIT.

Source: SDR IVSA075461 · FAA SDRS
O · 2001-08-06 Matched by certificate designator
N166DL · ATA 3340

PILOT REPORTED ANTI COLLISION LIGHT INOP. FLASH TUBE FOUND BURNED AND CRACKED. REPLACEMENT TUBE ORDERED AND INSTALLED. OPS CHECKED OK.

Source: SDR IVSA074819 · FAA SDRS
L · 1998-08-05 Matched by certificate designator
N491SA · ATA 3350

THE FIRST CLASS AND FWD SECTION OF COACH HAD EGRESS LIGHTING INOPERATIVE. FOUND POWER FEEDER LEAD LOOSE. RESECURED CONNECTOR. CHECK-C 3-12-98 STL.

Source: SDR TWAA9812701 · FAA SDRS
O · 1998-06-23 Matched by certificate designator
N491SA · ATA 5311

STL - ON LT Z14 RADIAL OTBD LOWER HOLE ON THE FORWARD SIDE, A .25 INCH CRACK WAS INDICATED BY EDDY CURRENT IN THE ATTACH ANGLE. REPAIRED PER ARA 15188. CHECK-C 3-12-98 STL. ACFT TT: 66,639 HOURS. ACFT TC: 80,202. (X)

Source: SDR TWAA9810310 · FAA SDRS
O · 1998-06-21 Matched by certificate designator
N491SA · ATA 5311

STL - THE RT Z34 RADIAL OUTBOARD LOWER HOLE ON FORWARD SIDE SHOWED CRACK INDICATION BY EDDY CURRENT. REPAIRED PER ARA 15188. CHECK-C 3-12-98 STL. ACFT TT: 66,639 HOURS. ACFT TC: 80,202. (X)

Source: SDR TWAA9810306 · FAA SDRS
O · 1998-06-21 Matched by certificate designator
N491SA · ATA 5311

STL - THE RT Z34 RADIAL WAS CRACKED ON END ABOUT 1 INCH. REPAIRED PER ARA 15188. CHECK-C 3-12-98 STL. ACFT TT: 66,639 HOURS. ACFT TC: 80,202. (X)

Source: SDR TWAA9810307 · FAA SDRS
O · 1998-06-21 Matched by certificate designator
N491SA · ATA 5320

STL - FOUND UPPER END FITTING ON AFT PRESSURE BULKHEAD RT Z34 RADIAL CRACKED .1250 INCH AT TEE FITTING. REPAIRED PER ARA 15188. CHECK-C 3-12-98 STL. ACFT TT: 66,639 HOURS. ACFT TC: 80,202. (X)

Source: SDR TWAA9810308 · FAA SDRS
O · 1998-06-21 Matched by certificate designator
N491SA · ATA 5311

STL - FOUND LT Z14 RADIAL OTBD UPPER HOLE ON THE FORWARD SIDE WITH .3750 INCH CRACK INDICATION BY EDDY CURRENT. REMOVED AND REPLACED END CLIP PER SRM 51-30-5, AND ARA 15188. CHECK-C 3-12-98 STL. ACFT TT: 66,639 HOURS. ACFT TC: 80,202. (X)

Source: SDR TWAA9810309 · FAA SDRS
O · 1998-06-20 Matched by certificate designator
N491SA · ATA 5311

STL - THE LT Z24 RADIAL, UPPER INBD HOLE ON THE FORWARD SIDE SHOWED CRACK INDICATION BY EDDY CURRENT. REMOVED AND REPLACED FITTING PER ARA 15188. CHECK-C 3-12-98 STL. ACFT TT: 66,639 HOURS. ACFT TC: 80,202. (X)

Source: SDR TWAA9810305 · FAA SDRS
O · 1998-06-20 Matched by certificate designator
N491SA · ATA 5312

STL - FOUND BULKHEAD SKIN CRACKED .25 INCH AT LT BULKHEAD AT Z24L, ON OTBD TOP SIDE, SECOND HOLE FORM END. REPAIRED SKIN PER ARA 15189. CHECK-C 3-12-98 STL. ACFT TT: 66,639 HOURS. ACFT TC: 80,202. (X)

Source: SDR TWAA9810312 · FAA SDRS
O · 1998-06-20 Matched by certificate designator
N491SA · ATA 5312

STL - THE UPPER END FITTING ON AFT PRESSURE BULKHEAD LT Z24 RIB WAS CRACKED AT TEE FITTING. REMOVED AND REPLACED END FITTING PER ARA 15188. CHECK-C 3-12-98 STL. (X)

Source: SDR TWAA9810315 · FAA SDRS
O · 1998-06-19 Matched by certificate designator
N491SA · ATA 5311

STL - ON THE LT Z34 RADIAL UPPER OTBD HOLE ON THE FORWARD SIDE, A CRACK INDICATION WAS SHOWN BY EDDY CURRENT. REPAIRED PER TWA ARA 15188. CHECK-C 3-12-98 STL. ACFT TT: 66,639 HOURS. ACFT TC: 80,202. (X)

Source: SDR TWAA9810311 · FAA SDRS
O · 1998-06-18 Matched by certificate designator
N491SA · ATA 5311

STL - THE Z48 RADIAL FORMER RT SIDE WAS FOUND CRACKED 1 INCH LONG ON OTBD END. REPAIRED FORMER PER ARA 15188. CHECK-C 3-12-98 STL. ACFT TT: 66,639 HOURS. ACFT TC: 80,202. (X)

Source: SDR TWAA9810313 · FAA SDRS
O · 1998-06-18 Matched by certificate designator
N491SA · ATA 5312

STL - THE LOWER END FITTING ON AFT PRESSURE BULKHEAD LT Z34 RIB HAD A .3750 INCH CRACK AT TEE FITTING. REPAIRED PER TWA ARA 15188. CHECK-C 3-12-98 STL. (X)

Source: SDR TWAA9810314 · FAA SDRS
L · 1998-05-29 Matched by certificate designator
N491SA · ATA 3350

STL - FLT 404 - EMERGENCY EXIT SIGNS AT R1 AND L1 DOORS CAME ON IN FLIGHT. WOULD NOT RESET UNTIL SHORT FINAL. REPLACED FWD EMERGENCY EXIT SIGN BATTERY PACK. (M)

Source: SDR TWAA9808603 · FAA SDRS
N · 1997-12-01 Matched by certificate designator
N491SA · ATA 2612

MCI - FLT 588 - DURING FLIGHT, RIGHT ENGINE FIRE WARNING LIGHT FLICKERED. REPLACED THE LOWER FIRE DETECTOR LOOP ASSY. (M)

Source: SDR TWAA9714102 · FAA SDRS
J · 1997-11-21 Matched by certificate designator
N491SA · ATA 2750

STL - FLT 218 - AT 14,000 DURING DESCENT INTO STL, FLAPS UNCOMMANDED DEPLOYED TOWARD 10DGR AT 300 KTS, WITHIN 5 SECONDS WERE PLACED TO UP. ACCOMPLISHED CHECKS PER MM 5-51-0 PAGE 609 SECTION D FOUND OK FOR SERVICE. (M)

Source: SDR TWAA9713701 · FAA SDRS
L · 1996-05-15 Matched by certificate designator
N491SA · ATA 3350

STL - FLT 619 - DURING PRE-FLIGHT, EMERGENCY LIGHTS AND EGRESS LIGHTS WOULD NOT ILLUMINATE. FOUND SWITCH HAD BEEN LEFT IN THE ON POSITION. REPLACED BATTERY POWER PACKS, MFG PN 5822-2 AND VR4D. EMERGENCY LIGHTS AND EGRESS LIGHT SYSTEM OPERATION CHECKED NORMAL. CHECK C - 5-22-95 - STL. (X)

Source: SDR 96ZZZX3023 · FAA SDRS

Linked aircraft

N-numberMake / modelYearStatusLink basis
N491SAROBINSON HELICOPTER COMPANY R44 II2009Valid RegistrationMatched by certificate designator
N543SABELL 206BValid RegistrationMatched by certificate designator
N545SABELL 206L-31983Valid RegistrationMatched by certificate designator
N547SAAEROSPATIALE AS350B21988Valid RegistrationMatched by certificate designator
N549SAMatched by certificate designator
N892SAROBINSON HELICOPTER COMPANY R44 II2014Valid RegistrationMatched by certificate designator