N911UF

EUROCOPTER EC 155 B1 · 2013 · Valid Registration

Registered owner: MILTON S HERSHEY MEDICAL CENTER, PA (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
MED-TRANS CORPORATION (M3XA)Certificate holderMatched by certificate designator
AIR METHODS LLC (QMLA)Operator2009-03-05 – 2009-03-05Operator named in NTSB report

Accident & incident history

Inc · 2009-03-05 Operator named in NTSB report
AGUSTA A109E Minor injury Part 135AIR METHODS LLC
Source: NTSB case ERA09IA186

Maintenance disclosures

K J · 2020-12-23 Matched by certificate designator
ATA 2910

DURING PILOT TRAINING THE NR 1 HYDRAULIC SYSTEM INDICATION ILLUMINATED DURING FLIGHT. THE LOW HYDRAULIC WARNING INDICATION ILLUMINATED AND APROXIMATELY 10 SECONDS LATER THE HYDRAULIC SERVO LIGHT ILLUMINATED. PILOT LOWERED THE LANDING GEAR AND LANDED WITHOUT INCIDENT. MAINTENANCE TROUBLESHOT THE HYDRAULIC SYSTEM AND DISCOVERED THE HYDRAULIC PUMP PRESSURE LINE TO BE CHAFFED AND LEAKING. HYDRAULIC PUMP WILL BE REPLACED DUE TO RUNNING DRY, AS WELL AS, THE PUMP PRESSURE AND RETURN LINES. DURING THE INSPECTION AS TO THE LOSS OF HYDRAULIC FLUID, IT WAS DISCOVERED THAT THE RUBBER INSIDE PORTION OF AN ADEL CLAMP HAD DETERIORATED TO THE POINT OF CHAFFING THE PRESSURE LINE AND WAS THE CAUSE OF THE SUBSEQUENT DAMAGE.

Source: SDR M3XA20201222008 · FAA SDRS
J · 2018-02-16 Matched by certificate designator
ATA 6300

ON SHORT FINAL, CREW REPORTED A LOUD BANG FROM THE TRANSMISSION DECK, PILOT REPORTED A TRANSMISSION PRESSURE LIGHT ILLUMINATED. LANDED WITHOUT INCIDENT. ON THE MAINTENANCE INSPECTION, REVEALED THE OIL COOLER FAN DRIVE SHAFT HAD SHEARED AND CUT INTO THE OIL COOLER FINS AND OIL PASSAGES. THE TRANSMISSION WAS REMOVED FOR REPAIR.

Source: SDR M3XA2018021603 · FAA SDRS
K J · 2011-09-02 Matched by certificate designator
ATA 2821

ACFT DEPARTED FOR REVENUE FLIGHT. MX WAS NOTIFIED BY GROUND CREW OF POSSIBLE FUEL ON THE HELIPAD. NOTIFIED PILOT OF PRESSENCE OF FUEL AND ADVISED HIM TO LAND AS SOON AS POSSIBLE. UPON MX ARRIVAL AT ACFT, APPLIED POWER TO NR1 FUEL BOOST PUMP AND NOTICED FUEL LEAKING FROM NR1 FUEL FILTER HOUSING. REMOVED FUEL FILTER HOUSING AND REPLACED FUEL FILTER AND FUEL FILTER O-RING. REAPPLIED POWER TO ACFT, FUNCTIONAL CHECK OF NR1 FUEL BOOST PUMP COMPLETED. POST MX GROUND RUN REVEALED NO LEAKS FROM AREA. ACFT RETURNED TO SERVICE. MANAGEMENT WAS NOTIFIED AND ACFT WAS RETURNED TO SERVICE.

Source: SDR QMLA2011090211090 · FAA SDRS
K B · 2011-01-07 Matched by certificate designator
ATA 2810

THE PILOT AND MED CREW HAD JUST DEPARTED THEIR BASE HELIPAD. AFTER APPROX 2-3 SECONDS AFTER TRANSITIONING TO FWD FLIGHT, THE CREW SMELLED FUEL IN THE CABIN. THE FLIGHT WAS IMMEDIATELY ABORTED AS THE PILOT RETURNED THE ACFT TO THE HELIPAD. THE MECHANIC BEGAN TROUBLESHOOTING THE SOURCE OF THE PROBLEM WHICH LED HIM TO DRAIN THE FUEL, REMOVE THE CABIN INTERIOR, AND CONDUCT A VISUAL INSP OF THE ACFT FUEL CELLS FOR LEAKS AND OBVIOUS DAMAGE. THE MECHANIC WAS THEN ABLE TO FIND THAT THE FUEL BAFFEL LACING HAD FRAYED, ALLOWING THE FUEL TO SHIFT FORE AND AFT. THIS SUBSEQUENTLY ALLOWED THE FWD FUEL QUANTITY PROBE TO SHIFT FORE AND AFT WEAKENING THE FUEL CELL AT THAT CONNECTION. THIS WEAKENING ALLOWED RAW FUEL VAPORS TO ESCAPE WHEN THE ACFT TRANSITIONED INTO FWD FLIGHT. THE MECHANIC IS IN THE PROCESS OF REPLACING THE MAIN FUEL CELL. ONCE COMPLETE, THE ACFT IS EXPECTED TO RETURN TO SERVICE.

Source: SDR QMLA2011010711005 · FAA SDRS
B · 2010-12-31 Matched by certificate designator
ATA 2120

THE PILOT AND MEDICAL CREW ONBOARD THE ACFT ALL SMELLED A STRONG FUEL ODOR SHORTLY AFTER TAKEOFF. THE PILOT IMMEDIATELY RETURNED TO THE HANGAR THAT HE JUST DEPARTED TO HAVE MX LOOK INTO THE PROBLEM. THE MECHANIC TROUBLESHOT THE PROBLEM COULD NOT DUPLICATE ON THE GROUND UNDER GROUND POWER AND WITH ENGINES RUNNING. THE PILOT AND MECHANIC THEN DEPARTED THE HELIPORT FOR A 15 MINUTE FLIGHT WHICH DID NOT DUPLICATE THE PROBLEM EITHER. MECHANIC UPON RETURN TO THE HELIPAD PERFORMED ONE MORE POST FLIGHT INSP FOR THE PRESENCE OF FUEL. NONE WAS FOUND. THE ACFT WAS THEN RETURNED TO SERVICE.

Source: SDR QMLA2011123111001 · FAA SDRS
J · 2007-05-05 Matched by certificate designator
ATA 2911

ENROUTE TO SCENE CALL THE EMERGECY HYDRAULIC PRESSURE LIGHT ILLUMINATED. ABORTED THE MISSION AND RETURNED TO BASE. THE OPERATION CONTROL CENTER AND MAINTENANCE WAS NOTIFIED. REPLACED HYDRAULIC ACCUMULATOR GROUP P/N 109-0512-70-109 S/N 823 WITH A SERVICEABLE ACCUMULATOR GROUP SAME P/N NEW S/N 523. OPERATIONAL CHECK COMPLIED WITH, NO DEFECTS NOTED. THIA A/C IS FROM OUR GAINSVILLE, FL PROGRAM.

Source: SDR BAQA200700013 · FAA SDRS
O · 2004-11-10 Matched by certificate designator
ATA 6410

FOUND CRACK ON 1 SIDE OF T/R BLADE AT STA 540.00, CRACK EXTEND FROM DOUBLER BACK 4 INCHES ALONG STA 540. CORDWISE REF FIG. 1 OF AD 2002-25-51 AIRCRAFT WAS POST MOD. (K)

Source: SDR BAQ2005F00000 · FAA SDRS
L · 2004-03-01 Matched by certificate designator
ATA 7320

UNIT COULD NOT PASS FUEL CHECK. THIS IS ORIGINAL EQUIPMENT OFF OF THE ENGINE, TIMES DO MATCH UP TO OVERHAULS. REPLACED WITH SERVICABLE UNIT. 03/09/2004

Source: SDR BAQA093337 · FAA SDRS
N · 2003-12-03 Matched by certificate designator
ATA 2612

ENGINE UNDER CONTRACT. FALSE FIRE WARNINGS OCCUR WHEN IT IS DAMP. THIS IS BEING SENT BACK UNDER A MFG WARRANTY CLAIM. REPLACED WITH SERVICEABLE UNIT. 12/16/03

Source: SDR BAQA091532 · FAA SDRS
O · 2003-10-17 Matched by certificate designator
ATA 6220

PITCH HORN HAS PITS IN BOLT HOLES. REPLACED WITH SERVICEABLE UNIT.

Source: SDR BAQA089978 · FAA SDRS
O · 2003-06-27 Matched by certificate designator
ATA 7410

HIGH ENERGY GENERATOR PRODUCING INTERMITTENT SPARK. REPLACED WITH SERVICEABLE UNIT.

Source: SDR BAQA087888 · FAA SDRS
O · 2003-04-08 Matched by certificate designator
ATA 6220

BUSHING DEBONDED COMPLETELY (RED ARM). REPLACED WITH SERVICEABLE UNIT.

Source: SDR BAQA085931 · FAA SDRS
O · 2003-04-03 Matched by certificate designator
ATA 2435

STARTER GEN HAS BRUSHES AND COMMUTATOR WORN. HARD CARD ENCLOSED (2). REPLACED WITH SERVICEABLE UNIT.

Source: SDR BAQA085901 · FAA SDRS
O · 2003-01-08 Matched by certificate designator
ATA 6220

BALL JOINT WORN. BEARING CAME OF ON STARFLEX IN THE POSITION OF THIS BALL JOINT. REPLACED WITH SERVICEABLE UNIT.

Source: SDR BAQA082899 · FAA SDRS
O · 2003-01-08 Matched by certificate designator
ATA 6220

MAIN ROTOR STARFLEX BEARING CAME OFF. REPLACED WITH SERVICEABLE UNIT.

Source: SDR BAQA082898 · FAA SDRS
O · 2001-01-05 Matched by certificate designator
ATA 6520

INITIAL GRND RUN-UP, AFTER MJR INSP, A T/R GBX FAILURE WAS EXPERIENCED AFTER APPROX 15-20 MINUTES. AC JERKED SEVERAL TIMES ALONG THE YAW AXIS, WITH NR1 ENG RUNNING AT 68%NG AND NR2 AT 65%NG AN UNUSUAL NOISE WAS HEARD FRM TAIL ROTOR, SHUT DOWN WAS INITIATED, NOISE WORSENED. ROTOR BREAK WAS APPLIED WITHIN 10 REV OF COMING TO COMPLETE STOP FRM COAST DWN WITH ROTOR BREAK APPLIED, LOUD SQUEALING AND GRINDING NOISE WAS EMITTING FROM THE TAIL ROTOR AND COAST DWN CAME TO A RAPID BUT NOT SUDDEN STOP. INITIAL INSP REVEALED METAL PARTICLES ON TAIL ROTOR CHIP PLUG, OIL AND SPREAD FLEX COUPLING AT THE TAIL ROTOR OUTPUT FLNG FROM MAIN GBX. AFTER TR DWN & INSP, OUTER BRG OF INPUT HSG WAS DRY, GBX OIL LEVEL WAS FULL.

Source: SDR 20010130CW009 · FAA SDRS