TIMBERLAND HELICOPTERS, INC.

Part 135 operator · designator TLLA

Data confidence: Records are linked by certificate number, aircraft registration, or a name match that a reviewer has confirmed. Each record below shows how it was linked.

Also recorded as: TIMBERLAND HELICOPTERS, INC., Timberland Helicopters, Timberland Helicopters, Inc.

Accident & enforcement record

Events that happened, regardless of the operator's own reporting. Each links to its public source.

NTSB accidents & incidents

Acc · 2023-07-19 Operator named in NTSB report
AEROSPATIALE AS-355E TWIN STAR (N102UM) None injury Part 135

Operated by TIMBERLAND HELICOPTERS INC (per NTSB report)

Source: NTSB case WPR23LA278
Acc · 2013-10-28 Operator named in NTSB report
BELL 206B (N16673) Serious injury Part 91

Operated by Timberland Helicopters (per NTSB report)

Source: NTSB case WPR14CA052

FAA enforcement actions

FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.

Maintenance disclosure history

Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.

18 reports on file.

J · 2025-06-26 Matched by certificate designator
N355TH · ATA 7200

#1 ENGINE CHIP LIGHT ILLUMINATED DURING FLIGHT. PILOT LANDED AT FIRST SAFEST SPOT AT SOUTHWEST WYOMING REGIONAL AIRPORT WITH NO INCIDENT. GROUNDED AC. SENT MECHANIC OUT AND FOUND CHIPS ON UPPER MAG. PLUG ON GEARBOX

Source: SDR TLLA205070200139 · FAA SDRS
O · 2024-11-30 Matched by certificate designator
N249TH · ATA 5310

FOUND WORKING FASTENERS ON L/H UPPER LONGERON FITTING. AFTER INSPECTION FOUND HOLE OUT OF TOLERANCE. REPLACE L/H UPPER LONGERON

Source: SDR 2025FA0000138 · FAA SDRS
O · 2024-09-30 Matched by certificate designator
N249TH · ATA 5311

DURING 300 HOUR A/F INSPECTION FOUND A CRACK AT STATION 142 R/H SIDE ON THE UPPER FRAME NOT RELATED TO ANY INCIDENT OR ACCIDENT.

Source: SDR 2025FA0000137 · FAA SDRS
O · 2024-09-30 Matched by certificate designator
N249TH · ATA 5310

FOUND WORKING FASTENERS ON L/H UPPER LONGERON FITTING. AFTER INSPECTION FOUND HOLE OUT OF TOLERANCE. REPLACED L/H UPPER LONGERON

Source: SDR TLLA2025031400138 · FAA SDRS
O · 2024-09-30 Matched by certificate designator
N249TH · ATA 5311

DURING 300 HOUR AF INSPECTION FOUND A CRACK AT STATION 142 R/H SIDE ON THE UPPER FRAME. NOT RELATED TO ANY INCIDENT OR ACCIDENT

Source: SDR TLLA2050314000137 · FAA SDRS
O · 2019-04-17 Matched by certificate designator
N5000G · ATA 5310

DURING SCHEDULED INSPECTION WORKING RIVETS WERE FOUND IN CABIN ROOF STRUCTURE STATION 142. THIS IS A COMMON LOCATION FOR WORKING FASTENERS IN THE 206 SERIES AIRCRAFT, ESPECIALLY ON HIGH TIME FUSELAGES. DISCREPANT FASTENERS REPLACE IAW DER STRUCTURAL ENGINEERING REPORT FW-THI709-91 AND BHT-ALL-SRM SECTION 3.

Source: SDR TLLA20190417001 · FAA SDRS
O · 2018-07-17 Matched by certificate designator
N249AE · ATA 5320

DURING ROUTINE INSPECTION FOUND LOOSE AND WORKING RIVETS IN CABIN ROOF STRUCTURE STATION 142.71. THIS IS A COMMON AREA FOR WORKING FASTENERS IN THIS SERIES AIRCRAFT, ESPECIALLY ON HIGH TIME FUSELAGES. DISCREPANT FASTENERS REPLACED IAW DER STRUCTURAL SUBSTANTIATION DOCUMENT FW-TH1687-25 AND BHT-ALL-SRM SECTION 3.

Source: SDR TLLA2018071700001 · FAA SDRS
O · 2018-03-16 Matched by certificate designator
N5000G · ATA 5320

CRACKS AT SEAT-PAN ATTACHMENT NUTPLATE LOCATION ON TOP FRONT STIFFENER OF CREW SEAT FORWARD BULKHEAD. REPLACED IAW STANDARD RIVETING PRACTICES.

Source: SDR TLLA031618 · FAA SDRS
O · 2016-03-16 Matched by certificate designator
N5373U · ATA 5310

DURING DAILY INSPECTION, FOUND CRACKS IN THE ARFT CROSSTUBE SUPPORT STRUCTURE LOWER CORNERS AND STIFFENERS. THE CRACKS ARE COMMON IN THIS MODEL ACFT AND THE REPAIR PROCEDURES ARE DETAILED IN THE SRM BHT 206, SRM-1, REPAIR 5-2-1. THIS ACFT MAY HAVE HAD A HISTORY OF FLIGHT TRAINING USE WITH PREVIOUS OPERATORS.

Source: SDR TLLA2016040100001 · FAA SDRS
O · 2016-03-16 Matched by certificate designator
N5373U · ATA 5310

DURING DAILY INSPECTION, FOUND CRACKS IN THE AFT CROSSTUBE SUPPORT LOWER CORNERS AND STIFFENERS. THE CRACKS ARE COMMON IN THIS MODEL ACFT AND THE REPAIR PROCEDURES ARE DETAILED IN THE SRM BHT-206 SRM-1, REPAIR 5-2-1. ACFT MAY HAVE HAD A HISTORY OF FLIGHT TRAINING USE WITH PREVIOUS OPERATORS.

Source: SDR TLLA2016040100002 · FAA SDRS
O · 2016-01-22 Matched by certificate designator
N5373U · ATA 5310

DURING SCHEDULED ANNUAL INSPECTION, FOUND A CRACK EMANATING FROM ACCESS HOLE IN LOWER WEB OF ROOF BEAM AT BS 119.0. THIS AREA INSPECTION IS DETAILED IN MM1-5-29, 300 HR INSPECTION. THIS ACFT HAS A CARGO HOOK, BUT HAS NO HISTORY OF UNUSUAL FLIGHT PARAMETERS: THE CRACK APPEARS TO BE THE RESULT OF NORMAL STRUCTURAL STRESSES.

Source: SDR TLLA201602020001 · FAA SDRS
O · 2015-08-10 Matched by certificate designator
N5000G · ATA 5320

CRACKS RUN FROM 1ST RIVET TO EDGE OF FITTING, ABOUT .5". THE INSPECTION OF THIS PART IS SPECIFICALLY DETAILED IN MFG INSPECTION CHECKLIST. LIKELY CAUSE IS AGE OF ACFT.

Source: SDR TLL2015F00000 · FAA SDRS
O · 2015-08-02 Matched by certificate designator
N5000G · ATA 5302

DURING SCHEDULED 100 HR INSPECTION, FOUND UPPER LT FUSELAGE, SIDE TAILBOOM MOUNT FITTING, PN 206-031-329-103 CRACKED. INSPECTION OF THIS PART IS ROUTINE IN THE CHECKLIST FOR 100 HR INSPECTION, REF BHT-206L1-MM-1, 5/19, 5-20. THIS PART APPEARED TO BE ORIGINAL EQUIPMENT.

Source: SDR TLLL2016FA0000009 · FAA SDRS
O · 1999-07-29 Matched by certificate designator
N102UM · ATA 6320

MAIN ROTOR TRANSMISSION CHIP LIGHT CAME ON IN-FLIGHT WHILE LANDING AT ITS BASE OF OPERATION. MAINTENANCE REMOVED CHIP PLUG. SEVERAL CHIPS WERE FOUND ON PLUG. EXAMINED OIL FILTER METAL AND ALUMINUM WAS PRESENT IN FILTER. REMOVED BEVEL REDUCTION GEARBOX ON COMBINING GEARBOX FOR REPAIR. TSO: 2,359.4 HOURS. OVERHAUL IS 3,000 HOURS.

Source: SDR 99ZZZX3541 · FAA SDRS
O · 1999-04-23 Matched by certificate designator
N5000G · ATA 6320

THE NYLON RETAINER FOR THE PLANATARY GEAR BEARING WAS FOUND IN THE TRANSMISSION OIL SCREEN IN SMALL PIECES. SUBMITTER STATED THIS IS THE FOURTH TRANSMISSION IN THE LAST 6 MONTHS WITH THIS PROBLEM.

Source: SDR 99ZZZX2163 · FAA SDRS
O · 1998-02-28 Matched by certificate designator
N5000G · ATA 6320

UPON TEAR-DOWN OF TRANSMISSION FOR INSPECTION, SCREEN ASSY WAS FULL OF NYLON PIECES. INVESTIGATION REVEALED RETAINERS ON PLANETARY GEAR, 1 EACH, COMPLETELY MISSING AND, 2 EACH, CRACKED.

Source: SDR 99ZZZX900 · FAA SDRS
O · 1998-01-21 Matched by certificate designator
N5000G · ATA 6230

INSPECTION FOUND DRIVE LINK ASSY WITH EXCESSIVE PLAY AT TWO PLACES. SEE BELL MM L-3 FIG 62-21. ON TEAR DOWN, FOUND BEARINGS AND SPACERS WORN BEYOND LIMITS. TOTAL TIME OF PARTS, LESS THAN 1,000 HRS/1 YEAR SINCE REPLACEMENT.

Source: SDR 98ZZZX1265 · FAA SDRS
O · 1996-04-13 Matched by certificate designator
N5000G · ATA 6230

PLAY IN EXCESS OF .025 INCH AT TWO PLACES. SEE BELL MM L3, FIGURE 62.21. AT TEAR DOWN FOUND BEARINGS AND SPACERS WORN. TOTAL TIMES LESS THAN 1,000 HOURS AND 1 YEAR SINCE REPLACED.

Source: SDR 96ZZZX4183 · FAA SDRS

Linked aircraft

N-numberMake / modelYearStatusLink basis
N102UMAEROSPATIALE AS-355E TWIN STAR1981Valid RegistrationMatched by certificate designator
N102UMAEROSPATIALE AS-355E TWIN STAR1981Valid RegistrationOperator named in NTSB report
N16673Operator named in NTSB report
N249THBELL HELICOPTER TEXTRON 206L-11980Valid RegistrationMatched by certificate designator
N5000GBELL HELICOPTER TEXTRON 206L-11978Valid RegistrationMatched by certificate designator
N5373UBELL 206B1988Valid RegistrationMatched by certificate designator