RVR AVIATION LLC

Part 135 operator · designator V8XA

Data confidence: All records on this page are linked by a shared certificate number or aircraft registration (N-number).

Also recorded as: RVR AIR CHARTER, RVR AVIATION LLC

Accident & enforcement record

Events that happened, regardless of the operator's own reporting. Each links to its public source.

NTSB accidents & incidents

No NTSB accidents or incidents linked to this operator.

FAA enforcement actions

FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.

Maintenance disclosure history

Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.

5 reports on file.

N · 2019-01-25 Matched by certificate designator
N234BZ · ATA 3260

LG AIR/GND FAIL MESSAGE ON CLIMB OUT MESSAGE PERSISTED DESPITE CYCLING THE GEAR TWO TIMES DIVERTED TO KGPYT FOR LONG RUNWAYS FOLLOWED QRH PROCEDURE LANDED FLAPS 45 AFTER LANDING MESSAGE PERSISTED ON EICAS POWER AIRCRAFT DOWN THEN POWERED UP LG AIR/GND WENT AWAY.

Source: SDR V8XA201901260001 · FAA SDRS
O · 2018-06-13 Matched by certificate designator
N234BZ · ATA 2312

UPON CLIME OUT 4000 AGL NR 2 RMU DISPLAY, NR 2 COMM DISPLAYED DASHES, NR 2 TRANSPONDER DISPLAYED DASHES, NR 2 TCAS DISPLAYED DASHES. NR 1 RMU DISPLAY, NR 1 TRANSPONDER DISPLAYED DASHES, TCAS DISPLAYED DASHES. ATC REQUESTED IDENT FOR TRANSPONDERS CREW SWITCHED BETWEEN NR 1 AND NR 2 WITH NO RESPONSE FROM TRANSPONDERS. CREW CHECKED NR 2 COM WITH NO RESPONSE. CREW REQUESTED ATC TO RETURN TO ORIGINAL DESTINATION AIRCRAFT LANDED WITH NO ISSUES. PERFORMED TROUBLESHOOTING FOUND A PASTE LUBRICANT ON THE COAX CONNECTORS CLEANED AND RE-SEATED NAV/COM BOXES PERFORMED OPERATIONAL CHECKS AND TDR CHECKS WITH NO DEFECTS NOTED AT THIS TIME.

Source: SDR V8XA2018061500000 · FAA SDRS
B J · 2013-06-07 Matched by certificate designator
N926FM · ATA 3040

WINDSHIELD HEAT NR 2 FAIL MESSAGE APPEARED WHEN SELECTED ON DURING DESENT. ELECTRIC BURNING SMELL SHORTLY AFTER. FOLLOWED QRH PROCEDURES AND PERFORMED A NORMAL APPROACH AND LANDING. FOUND WINDOW HEAT CONTROLLER TO BE FAILED. PLACED WINDOW HEAT SYS ON MEL 30-42-02 AND PERFORMED SPECIAL PROCEDURES SP-30-42-02, PULLED AND SAFETIED THE WINDSHIELD TEMP CB J20. ALSO, FOUND WINDSHIELD TO BE DELAMINATED WITHIN MFG ALLOWABLE LIMITS. NO WINDSHIELD DELAMINATION NOTED WITHIN THE HEATED AREA. PLACED AOG ORDER FOR WINDOW HEAT CONTROLLER AND RT WINDSHIELD.

Source: SDR 7GMB201306070466 · FAA SDRS
B · 2009-04-30 Matched by certificate designator
N926FM · ATA 2520

ON CLIMB OUT, THROUGH APPROX 17,000, FLT ATTENDANT REPORTED THAT WHEN THE PC-POWER SYSTEM WAS TURNED ON, 1 PASSENGER MOMENTARILY SMELLED A FAINT ODOR, WHICH CAME & WENT QUICKLY, SMELLING LIKE ELECTRICAL SMOKE. NO OTHER PASSENGER IN THE AREA NOTED THE ODOR, NOR DID THE FLT ATTENDANT. AS A PRECAUTION, PC-POWER SYSTEM TURNED OFF. QRH PROCEDURES REVIEWED REGARDING SMOKE/ODOR IN CABIN, NO FURTHER ACTION REQUIRED. NO FURTHER ISSUES NOTED DURING FLT. MX POWERED UP ACFT ELECTRICAL SYS & OBSERVED FOR 1 HOUR. ALL INTERIOR SYS OPS NORMAL, NO ODORS NOTED. MULTIPLE OPS CHECKS OF PC-POWER SYS REVEALED SEATS 7BC DID NOT POWER UP & TEST PROPERLY. ENTIRE PC-POWER SYS PLACED ON MEL 25-60-02, PLACARDS AFFIXED & CIRCUIT BREAKERS PULLED & COLLARED. R & R ISPC IN ROW 7BC. INSPECTED WIRING & FOUND NO DEFECTS. SYS OPS FOR A TOTAL OF 1 HOUR 45 MINUTES WITH NO DEFECTS NOTED. AMM TASK 24-20-05-400-801-A SYS HAS BEEN REACTIVATED, CB RESET & PLACARDS REMOVED. CLEARED MEL 25-60-02.

Source: SDR I06B20090501FM · FAA SDRS
O · 2008-10-30 Matched by certificate designator
N926FM · ATA 5280

14K FT NOTICED A FLASH OF LIGHT THAT APPEARED TO BE BELOW THE AIRCRAFT. THE CREW REPORTED NO AIRCRAFT ANOMALIES AS A RESULT OF THE SUSPECTED NEAR LIGHTNING STRIKE. FO PERFORMED THE POST FLT INSP AND IMMEDIATELY NOTICED A PIN HOLE IN THE NOSE GEAR DOOR. CAPTAIN CONFIRMED AIRCRAFT HAD BEEN STRUCK BY LIGHTNING. THE REMOVAL OF THE AILERON WAS INITIATED. THE ALTERNATIVE TO MOVE THE PART TO THE UNITED AIRLINES COMPOSITE REPAIR SHOP IN SFO WAS EXECUTED. REPAIRS WHERE MADE PER THE STRUCTURAL REPAIR MANUAL, AND AN ASG MECHANIC REMAINED IN THE AREA TO TRANSPORT THE REPAIRED PARTS TO MHR. THE AIRCRAFT HAD ALL OF THE BELLY REWORK ACCOMPLISHED DURING THE SAME TIME PERIOD. REINSTALLATION WAS ACCOMPLISHED AND THE REQUIRED INSPECTIONS COMPLETED AND SIGNED.

Source: SDR I06B20081030001 · FAA SDRS

Linked aircraft

N-numberMake / modelYearStatusLink basis
N234BZEMBRAER EMB-135LR2001Valid RegistrationMatched by certificate designator
N311RFMatched by certificate designator
N403RWEMBRAER EMB-135LR2000Valid RegistrationMatched by certificate designator
N618LTMatched by certificate designator
N717VLCESSNA 5602008Valid RegistrationMatched by certificate designator
N831RWDASSAULT-BREGUET FALCON 501985Valid RegistrationMatched by certificate designator
N926FMEMBRAER EMB-135ER2001Valid RegistrationMatched by certificate designator