CROW EXECUTIVE AIR, INC.

Part 135 operator · designator DRUA

Data confidence: All records on this page are linked by a shared certificate number or aircraft registration (N-number).

Also recorded as: CROW EXECUTIVE AIR, INC., Crow Executive Air, Inc., ISRAFLY

Accident & enforcement record

Events that happened, regardless of the operator's own reporting. Each links to its public source.

NTSB accidents & incidents

No NTSB accidents or incidents linked to this operator.

FAA enforcement actions

FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.

Maintenance disclosure history

Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.

14 reports on file.

O · 2010-02-11 Matched by certificate designator
N325NW · ATA 5321

DURING "H" CHECK FOUND FLOOR PANEL 261EF DELAMINATED. REPLACED FLOOR PANEL. WORK ACCOMPLISHED IAW DWG 3D25-37498.

Source: SDR DALA103453225 · FAA SDRS
O · 2010-02-11 Matched by certificate designator
N325NW · ATA 5321

DURING "H" CHECK FOUND FLOOR PANEL 231FF HAS BROKEN CORNERS. REPLACED FLOOR PANEL. WORK ACCOMPLISHED IAW DWG 3D25-37498.

Source: SDR DALA103463225 · FAA SDRS
O · 2010-02-11 Matched by certificate designator
N325NW · ATA 5321

DURING "H" CHECK FOUND FLOOR PANEL 231CF HAS CORRODED INSERTS AND A TORN EDGE. REPLACED FLOOR PANEL. WORK ACCOMPLISHED IAW DWG 3D25-37498.

Source: SDR DALA103473225 · FAA SDRS
O · 2009-08-19 Matched by certificate designator
N325NW · ATA 2910

LINE HAD CORROSION ON 90 DEGREE BENDS ADJACENT TO FERRULES FOR B-NUTS. THE PORTION OF THE LINE AT BOTH ENDS HAD CORROSION THA WAS PRESENT WHERE THE PROTECTIVE COATING WAS REMOVED, APPARENTLY DURING MFG OF THE PART. THE CORROSION HAD EATEN THROUGH ONE END OF THIS LOCATION SUFFICIENT TO REDUCE WALL THICKNESS ALLOWING LINE TO BURST.

Source: SDR 2009FA0000766 · FAA SDRS
N · 2005-02-14 Matched by certificate designator
N88FA · ATA 7714

LT ENGINE FAILED TO START NORMALLY. IN MANUAL MODE START WAS SUCCESSFUL. SUBSEQUENT START, GENERATOR WAS INOPERATIVE. EXTENSIVE TROUBLESHOOTING FINALLY DETERMINED THAT THE STARTER-GENERATOR HAD SIEZED, STRIPPING PLASTIC DRIVE ADAPTER IN ENGINE. DRIVE ADAPTER WAS REPLACED, ALONG WITH A SERVICEABLE STARTER-GENERATOR, SYSTEMS FUNCTION NORMALLY.

Source: SDR 2005F00038 · FAA SDRS
H · 2005-01-04 Matched by certificate designator
N88FA · ATA 2435

LEFT ENGINE FAILED ROTATE DURING START SEQUENCE INITIATION. MAINTENANCE DETERMINED BRUSHES BURNT, APPROXIMATELY 50 PERCENT LENGTH/LIFE REMAINING. STARTER/GENERATOR WAS REPLACE, ALONG WITH DC VOLTAGE REGULATOR. NR 1 INVERTER HAD FAILED COUPLE DAYS PRIOR, NO INDICATION ONE FAILURE CONTRIBUTED TO OTHER.

Source: SDR 2005FA0000009 · FAA SDRS
J · 2004-12-21 Matched by certificate designator
N88FA · ATA 3233

DURING TAKEOFF, LANDING GEAR FAILED TO RETRACT, THEN FAILED TO EXTEND, WAS MANUALLY EXTENDED VIA EMERGENCY PROCEDURES. MAINTENANCE DISCOVERED LANDING GEAR MOTOR CIRCUIT BREAKER TRIPPED, MOTOR ITSELF SUFFERED INTERNAL HEAT DAMAGE. TIME IN SERVICE SINCE OVERHAUL, 78 HOURS.

Source: SDR 2004F00439 · FAA SDRS
N · 2004-01-13 Matched by certificate designator
N7810W · ATA 2612

FALSE FIRE WARNING DURING FLIGHT. AFTER THE AIRCRAFT LANDED, THE PILOT REPORTED THAT THE INDICATION WAS INTERMITTENT. THE RT ENGINE COWLING WAS REMOVED, AND THE ENGINE WAS INSPECTED. THERE WAS NO INDICATION OF FIRE IN THE ENGINE AREA. THE FIRE LOOP LOOKED OK, NO DAMAGE NOTED. NOT HOT SPOTS ON THE ENGINE WERE NOTED, FROM BLEED AIR LINES OR OTHERWISE. THE WIRING CONNECTIONS AT THE NACELLE FIREWALL WERE DISCONNECTED, AND THERE APPEARED MORE THAN NORMAL BUILD UP OF GRIME AND CARBON. CLEANED THE TERMINALS AND CONTACTS. RECONNECTED THE WIRES. RAN THE AIRCRAFT WITHOUT AND WITH THE COWLINGS ON, COULD NOT DUPLICATE THE FALSE FIRE INDICATION.

Source: SDR DRU2004F00000 · FAA SDRS
O · 2003-02-10 Matched by certificate designator
N7810W · ATA 3010

DURING INSP BY MECH, A BLACK STREAK (FORE TO AFT) WAS NOTICED ON LT HORIZ STAB, THAT BOOT LOOKED BURNT ON L.E. EXAMINATION REVEALED THAT BOOT MUST HAVE SHORTED AGAINST L.E., BURNING BOTH BOOT AND HORIZ STAB CONSISTED OF NICKEL SIZE HOLE BEING COMPLETELY BURNT THROUGH. NO OTHER INTERNAL STRUCTURES WERE DAMAGED. BOTH BOOT AND L.E. SKIN WERE REMOVED AND REPLACED BY NEW COMPONENTS. LAST SCHEDULED INSP OF TAIL REVEALED NO ANNOMOLIES. AN INSPECTION OF STAB DE-ICE SYST WAS ACCOMPLISHED, INCLUDING SEQUENCE TIMER, WIRING, CIRCUIT BREAKERS, CURRENT LIMITER, TERMINAL BLOCKS, SYST SWITCH, AND CAUTION LIGHT. PILOTS REPORTED NO DISCREPANCIES. CIRCUIT BREAKERS AND CURRENT LIMITER HAD NOT BLOWN PREVENTING THIS MALFUCTION.

Source: SDR DRU2003F00000 · FAA SDRS
O · 2002-03-06 Matched by certificate designator
N43TJ · ATA 7500

WHILE TROUBLESHOOTING THE BLEED AIR HEATING SYSTEM, WHICH WAS INOPERATIVE, SOME LEAK CHECK SOLUTION HAD GOTTEN ON HEATING SENSOR AND CONTROL HOSES. HOSES WERE LEAKING. REMOVED OLD SENSOR AND CONTROL HOSES, AND INSTALLED NEW HOSES. LEAK CHECK WAS GOOD, AND SYSTEM FUNCTIONAL CHECK WAS GOOD. HOSES USED IN THIS PORTION OF SYSTEM WERE 303-4 HIGH PRESSURE HOSE, DATE CODE WAS 3/76, MOST LIKELY ORIGINAL. VISUALLY HOSES LOOKED ACCEPTABLE, AND THE FLEXIBILITY WAS GOOD, BUT DUE TO HOSES AGE, HAD DETERIORATED, COULD NOT MAINTAIN PRESSURE EVEN AT LOW OPERATING PRESSURES OF THIS SYSTEM. SOME OF THE ORFICED (T) FITTINGS INSTALLED IN THE SYSTEM WERE CLOGGED.

Source: SDR DRU2002F00000 · FAA SDRS
A · 2001-04-27 Matched by certificate designator
N4078L · ATA 7314

DURING LANDING ROLLOUT, AN EXPLOSION AND FIRE OCCURRED IN LEFT ENGINE. EXAMINATION FOUND THE FUEL PUMP RELIEF VALVE COVER GASKET LEAKING FUEL. AD AND SB HAD BEEN ACCOMPLISHED SEVERAL HUNDRED HOURS AGO. THE DAMAGE WILL REQUIRE REPLACEMENT OF ALL ENGINE ASSEMBLY, ENGINE, TURBOMOUNT, TOP COWL. PUMP WAS RECEIVED NEW WITH ENGINE.

Source: SDR 20010511CW004 · FAA SDRS
O · 1997-07-30 Matched by certificate designator
N4078L · ATA 2460

DURING AN EVENT INSPECTION, SB 1004 WAS C/W. THE FINDINGS OF THE INSPECTION MIRRORED THAT OF THE SERVICE BULLETIN, IN THAT, YES, THE CONNECTOR WAS BURNT AND HAD DISTORTED. PART WAS REMOVED AND REPLACED IAW INSTRUCTIONS PROVIDED IN SB 1004. NO INCIDENT HAD RESULTED FROM THE ABOVE PROBLEM.

Source: SDR 97ZZZX3681 · FAA SDRS
O · 1996-02-13 Matched by certificate designator
N119MA · ATA 3244

TIRE DEVELOPED A BULGE IN SIDEWALL AFTER A SHORT TIME IN SERVICE.

Source: SDR 96ZZZX957 · FAA SDRS
O · 1996-02-13 Matched by certificate designator
N740EJ · ATA 3244

TIRE DEVELOPED A BULGE IN THE SIDEWALL AFTER A SHORT TIME IN SERVICE.

Source: SDR 96ZZZX958 · FAA SDRS

Linked aircraft

N-numberMake / modelYearStatusLink basis
N325NWGATES LEARJET CORP. 35A1980Valid RegistrationMatched by certificate designator
N88FABEECH B1001979Valid RegistrationMatched by certificate designator