WHITE CLOUD CHARTER LLC

Part 135 operator · designator WH6A

Data confidence: All records on this page are linked by a shared certificate number or aircraft registration (N-number).

Also recorded as: WHITE CLOUD CHARTER LLC, White Cloud Charter LLC

Accident & enforcement record

Events that happened, regardless of the operator's own reporting. Each links to its public source.

NTSB accidents & incidents

No NTSB accidents or incidents linked to this operator.

FAA enforcement actions

FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.

Maintenance disclosure history

Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.

3 reports on file.

P · 2019-12-03 Matched by certificate designator
N555LR · ATA 3412

ORIGINAL FAILURE OF PROBE NOTED ON CAS 10/02/19 S/N A96142. REPLACEMENT TAT S/N B456 (INSPECTED/TESTED) FAILED 10/28/19. REPLACEMENT TAT S/N B821 (REPAIRED)FAILED 11/06/19. REPLACED WITH S/N A67219. (REPAIRED) GOOD SO FAR. WE HAVE HAD 3 REPAIRED PROBES FAIL IN SHORT TIME AND HAVE PROVEN THEM BAD BY PUTTING THEM ON BOTH SIDES OF THE AIRCRAFT.

Source: SDR WH6A2019120631098 · FAA SDRS
O · 1996-06-24 Matched by certificate designator
N601WW · ATA 2133

APPROX TWO HOURS INTO FLIGHT, CABIN PRESSURIZATION BEGAN TO FLUCTUATE 300 FEET IN AUTO MODE. AIR RUSHING NOISE COULD BE HEARD IN BAGAGE AREA. THE ELECTRO/PNEUMATIC OUTFLOW VALVE WAS REPLACED DURING AT 1200 HOUR INSPECTION APPROXIMATELY (8) FLIGHT HOURS PRIOR. PRESSURIZATION IS OK IN MANUAL MODE. AIRCRAFT DIVERTED TO BOMBARDIER IN TUCSON, AZ. OUTFLOW VLV WAS REPLACED. THE ORIGINAL INSTALLED WAS PREVIOUSLY REPAIRED FOR INTERMITTENT PRESSURIZATION FLUCTUATION.

Source: SDR 96ZZZM1323 · FAA SDRS
J M · 1996-03-17 Matched by certificate designator
N601WW · ATA 7261

FIRE WARNING INDICATION ON RT ENGINE AND REPORTED THROTTLE POWER LESSENED WHILE AT CRUISE. RESTARTED, THROTTLE WARNING WENT OUT. UNSCHEDULED LANDING AT ICT. ENGINE WAS NOT SHUT DOWN. FOUND FUEL DRAIN LINE FROM FUEL FLOW DIVIDER DISCONNECTED AND NR 4 AND NR 5 BEARING PACKAGE OIL INLET TUBE CHAFED THROUGH DUE TO LOOSE BOLTS IN 4TH TURBINE NOZZLE VANE HITTING TUBE. RETORQUED AND RESAFTIED ALL RETENSION VANE BOLTS. REPLACED CHAFED OIL TUBE. C/W ALLIED SIGNAL SB ALF 502-72-008, REV 8, AD 80-22-53, SB ALF 502-72-0221 WELDS RETENSION BOLT HEADS AS A SAFETY.

Source: SDR 96ZZZX1690 · FAA SDRS

Linked aircraft

N-numberMake / modelYearStatusLink basis
N999LRGULFSTREAM AEROSPACE GV-SP (G550)2014Valid RegistrationMatched by certificate designator