THE WHITEWIND COMPANY

Part 135 operator · designator UWUA

Data confidence: All records on this page are linked by a shared certificate number or aircraft registration (N-number).

Also recorded as: THE WHITEWIND COMPANY, The Whitewind Company

Accident & enforcement record

Events that happened, regardless of the operator's own reporting. Each links to its public source.

NTSB accidents & incidents

No NTSB accidents or incidents linked to this operator.

FAA enforcement actions

FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.

Maintenance disclosure history

Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.

8 reports on file.

N · 2012-02-15 Matched by certificate designator
N838SC · ATA 3240

AIRCRAFT DEPARTED KBDL AT 0900 LOCAL TIME. DURING LANDING GEAR EXTENSION ON APPROACH TO KHPN CREW GOT A NR 1 BRAKE OVERHEAT INDICATION. AIRCRAFT RETURNED TO KBDL AND MADE AN UNEVENTFUL LANDING. THE NR 1 BRAKE TEMP SENSOR WAS REPLACED AND THE AIRCRAFT RETURNED TO SERVICE.

Source: SDR UWUA02152012 · FAA SDRS
O · 2011-09-07 Matched by certificate designator
N711LS · ATA 5610

(CAN) EXPERIENCED A CRACK IN THE RT WINDSHIELD. THE FLIGHT CREW REPORTED THAT THE INITIAL CRACK OCCURRED IN FLIGHT AND WAS A SINGLE CRACK ALONG THE CENTER POST AND BOTTOM. THE FLIGHT CREW REPORTED THAT THE WINDSHIELD HEAT FAILED AT THE SAME TIME. SUBSEQUENTLY, SEVERAL OTHER CRACKS DEVELOPED SURROUNDING THE OUTSIDE EDGE OF THE WINDOW. EXAMINATION OF THE INTIAL CRACK SHOWED THAT IT ALSO HAD A BURN MARK IN IT. THERE WERE NO INJURIES REPORTED. THE WINDSHIELD HAS BEEN REPLACED.

Source: SDR CA110913001 · FAA SDRS
O · 2011-05-05 Matched by certificate designator
N711LS · ATA 5610

12 MINUTES AFTER DEPARTURE THE PILOT'S WINDSHIELD FACE PLY CRACKED IN SEVERAL PLACES. THE AIRCRAFT RETRUNED TO DEPARTURE AND MADE AN UNEVENTFUL LANDING. THE WINDSHIELD WAS REPLACED AND THE AIRCRAFT RETURNED TO SERVICE.

Source: SDR 2011F00116 · FAA SDRS
O · 2002-03-01 Matched by certificate designator
N247WF · ATA 2460

AIRCRAFT ESS BUSS FILED, MESSAGE DISPLAYED ON ED NR 1, TROUBLESHOT PROBLEM TO AN INTERMITTENT AC ESS BUSS SENSE RELAY (K1XD) IN JB 18. REPLACED RELAY (K1XD), OPS TEST AC ESS BUSS SYSTEM, NO FAULTS NOTED. NOTE: ESS BUSS DID NOT FAIL, SENSE RELAY FAILED GIVING AN INDICATION OF A FAILED ESS BUSS WAS ALWAYS POWERED.

Source: SDR UWU2002F00000 · FAA SDRS
O · 2002-03-01 Matched by certificate designator
N818TH · ATA 5210

MAIN ENTRANCE DOOR SUPPORT FOOT COLLAPSED. REPLACED MAIN DOOR ACTUATING ROD AND FOOT SUPPORT FOAM. OPS CHECKED MAIN DOOR NORMAL, NO FAULTS NOTED. NOTE: MAIN DOOR FOOT SUPPORT FOAM WAS MISSING CAUSING FOOT TO STICK IN POCKET, CAUSING ROD TO BREAK.

Source: SDR UWU2002F00001 · FAA SDRS
K J · 2001-01-16 Matched by certificate designator
N708SC · ATA 2913

WHILE AT CRUISE, THE CREW OBSERVED NR 2 HYD SYSTEM QTY WAS LOW. CREW MONITORED NR 2 HYD SYSTEM QUANTITY AND TEMPERATURE, HYD TEMP ROSE ABOVE 135 DEGREES CELSIUS AND QUANTITY DEPLETED TO ZERO. CREW SHUT DOWN NR 2 ENGINE PER CNDAIR ''QUICK REF HANDBOOK'' ABNORMAL PROCEDURES SECT 10. CREW DIVERTED A/C TO IRELAND AND LANDED WITHOUT INCIDENT. UPON INSPECTION OF NR 2 HYD SYSTEM, FOUND RT ENGINE DRIVEN HYD PUMP LEAKING HYD FLUID FROM ENGIEN GANG DRAIN. REPLACED NR 2 ENGINE DRIVEN HYD PUMP AND CASE DRAIN FILTER IAW A/C MM. A/C RETURNED TO SERVICE. (M)

Source: SDR 20010216SG008 · FAA SDRS
B · 1998-12-15 Matched by certificate designator
N818LS · ATA 3820

AFTER TAXI AND ENGINE SHUT DOWN WITH APU OPERATING, FLIGHT CREW NOTED STRONG ODOR FROM CABIN AREA. FURTHER INVESTIGATION REVEALED ODOR EMANATING FROM LAVATORY VANITY AREA. CREW IMMEDIATELY REMOVED ELECTRICAL POWER FROM AIRCRAFT. AIRCRAFT WAS SENT TO MAINTENANCE FACILITY FOR DETAILED INSPECTION. UPON VANITY ACCESS, PARTIAL DISASSEMBLY AND INSPECTION POTABLE WATER HEATER BLANKET SEVERELY OVERHEATED. ALSO, NOTED WAS THE INTERNAL BLANKET WIRES WERE CHAFED BY CLAMP THAT SECURES HEATING BLANKET TANK ASSEMBLY TO STRUCTURE. MINOR REPAIRS WERE MADE TO DAMAGED INSULATION ADJACENT TO HEATING BLANKET. SYSTEM DE-ACTIVATED PER MEL AND RELEASED.

Source: SDR 99ZZZX838 · FAA SDRS
E · 1998-03-29 Matched by certificate designator
N818TH · ATA 7250

HPN - NORMAL TAKEOFF EN ROUTE BAHAMAS. APPROX 1 HR EN ROUTE AT FL 310, PILOT NOTED NR 1 ENG VIBRATION INCREASE FROM .3 M/S TO .6 M/S AND INCREASE IN ENG NOISE. ALL OTHER ENG INDICATIONS WITHIN NORMAL PARAMETERS. ENG NOISE SUBSIDED THEN INCREASE IN ENG VIBRATION FROM .6 M/S TO .9 M/S, WITHIN NORMAL LIMITS. PILOT DISCONTINUED FLT, PRECAUTIONARY LANDING AT ISP. BORESCOPE INSP REVEALED NR 2 TURB DISC DAMAGE. ENG REMOVED AND REPLACED. UPON ENG DISASSY AND REPAIR, ALLIED SIGNAL NOTED A GAS PRODUCER SPACER WAS INSTALLED. SPACER CONFIG IS NOT COMPATIBLE WITH ALF502L-2C ENGINES AND THEY SUSPECT ENG DAMAGE A DIRECT RESULT OF INSTALL OF INCORRECT GAS PRODUCER SPACER CONFIG. ENG REPAIRED AND RETURNED TO SERVICE.

Source: SDR 98ZZZX3215 · FAA SDRS

Linked aircraft

N-numberMake / modelYearStatusLink basis
N18LSMatched by certificate designator
N711LSMatched by certificate designator
N717MKMatched by certificate designator
N74WWEXCLUSIVEUSEMatched by certificate designator
N811LSCESSNA 208B2010Valid RegistrationMatched by certificate designator
N838SCMatched by certificate designator
N878SCBOMBARDIER INC BD-700-1A102014Valid RegistrationMatched by certificate designator