SP Air Corporation

Part 135 operator · designator SQPA

Data confidence: All records on this page are linked by a shared certificate number or aircraft registration (N-number).

Also recorded as: SP Air Corporation

Accident & enforcement record

Events that happened, regardless of the operator's own reporting. Each links to its public source.

NTSB accidents & incidents

Acc · 2015-09-06 Matched by aircraft (N-number)
CESSNA T210L (N732DW) None injury Part 91
Source: NTSB case GAA15CA259
Accident · 1998-07-29 Matched by aircraft (N-number)
Cessna TU206G (N756YC) Minor injury
Source: NTSB case SEA98TA152
Accident · 1993-05-25 Matched by aircraft (N-number)
Cessna TU206G (N5203X) None injury
Source: NTSB case SEA93LA122

FAA enforcement actions

FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.

Maintenance disclosure history

Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.

10 reports on file.

O · 2019-09-17 Matched by certificate designator
N52095 · ATA 3242

PISTON IN LH BRAKE CALIPER LOCKED IN PLACE CAUSING THE BRAKE TO DRAG, PILOT ABORTED TAKE OFF TO CHECK BRAKES. WE BELIEVE THIS WAS CAUSED BY WORN BRAKE PADS. NO EMERGENCY MEASURES TAKEN. NO SBS, ADS, ICAS OR STCS APPLY. BRAKE PADS WERE WITHIN TOLERANCE, BUT WE BELIEVE REPLACING THEM SOONER SHOULD PREVENT THIS FROM OCCURRING.

Source: SDR SQPA20190919003 · FAA SDRS
D · 2019-08-13 Matched by certificate designator
N73TG · ATA 5280

LT GEAR DOOR BUCKED IN FLIGHT. SUSPECT GEAR DOOR WAS DAMAGED DUE TO OVERSPEED. NO WORK RECENTLY PERFORMED ON LANDING GEAR. NO EMERGENCY ACTIONS TAKEN. NO APPLICABLE ADS, SBS, STCS OR ICAS. SUGGEST VISUAL INSPECTION OF ADHESIVE ATTACHING STRUCTOR TO DOOR EVERY 50HRS OR AFTER SUSPECTED/REPORTED GEAR OVERSPEED.

Source: SDR SQPA20190919001 · FAA SDRS
O · 2019-08-13 Matched by certificate designator
N732DW · ATA 3222

NOSE GEAR CAME LOOSE FROM NOSE GEAR FORK. NOSE GEAR BOLT FORK FOUND TO BE MISSING. NO WORK RECENTLY PERFORMED ON NOSE GEAR. NO EMERGENCY MEASURES TAKEN. NO ADS, SBS, STCS OR ICA'S APPLY. BOLT WAS NOT FOUND POST EVENT. SUGGEST PREFLIGHT INSPECTION TO ENSURE BOLT IS SECURE AND IN PLACE.

Source: SDR SQPA20190919002 · FAA SDRS
D · 2017-03-20 Matched by certificate designator
N114BH · ATA 6110

LEFT PROPELLER DEPARTED AIRCRAFT DURING CLIMBOUT. NO PRIOR INDICATION OF PROBLEMS WERE REPORTED BY PILOT

Source: SDR SQPA032020170001 · FAA SDRS
O · 2011-08-29 Matched by certificate designator
N6993N · ATA 8530

PILOT REPORTED LOUD BANG ON CLIMBOUT. RETURNED WITHOUT INCIDENT TO FIELD. UPON EXAMINATION FOUND NR 4 CYLINDER HEAD SEPARATED FROM CYLINDER AT 5TH COOLING FIN ON HEAD. ENGINE TSO AND CYLINDER TSN 817.6 HRS. LAST COMPRESSION CHECK WAS AT 100 HR INSPECTION 19.2 HRS PRIOR WITH COMPRESSION 69/80.

Source: SDR SQP2011F00000 · FAA SDRS
B H · 2000-08-02 Matched by certificate designator
N9912Q · ATA 2410

PILOT DEPARTED BOISE, NOTICED SMOKE IN THE COCKPIT AND RETURNED FOR LANDING. ALTERNATOR CIRCUIT BREAKER FAILED (DUE TO AGE). NO OTHER DAMAGE FOUND. (X)

Source: SDR 20000908SH005 · FAA SDRS
O · 1996-01-26 Matched by certificate designator
N756WZ · ATA 5751

THE LT AND RT OUTBOARD AILERON HINGES WERE FOUND CRACKED AT THE LOWER MOUNTING FLANGE AREA. SUBMITTER ASSUMES FATIGUE AS CAUSE AND RECOMMENDS CAREFUL INSPECTION OF HINGE THROUGH THE TRAILING EDGE FALSE SPAR.

Source: SDR 96ZZZX861 · FAA SDRS
O · 1996-01-26 Matched by certificate designator
N756WZ · ATA 5751

THE LT AND RT OUTBOARD AILERON HINGES WERE FOUND CRACKED AT THE LOWER MOUNTING FLANGE AREA. SUBMITTER ASSUMES FATIGUE AS CAUSE AND RECOMMENDS CAREFUL INSPECTION OF HINGE THROUGH THE TRAILING EDGE FALSE SPAR.

Source: SDR 96ZZZX862 · FAA SDRS
O · 1995-12-15 Matched by certificate designator
N592GC · ATA 7810

FOUND SMALL HOLE IN CENTER OF THE LT EXHAUST AFT ELBOW WHILE C/W AD 75-23-08R5, EFFECTIVE DATE 11-4-86. THIS PART HAS BEEN INSTALLED ON THIS C-340 L.A.W. RAM STC SA234SW. SAID PART IS LISTED IN TABLE III OF AD 75-23-08R5 AS AN EXEMPT COMPONENT PER PART I(A). SUBMITTER RECOMMENDATION WOULD BE TO EXCLUDE THIS PART FROM THE EXEMPT LIST.

Source: SDR 96ZZZX93 · FAA SDRS
O · 1995-05-24 Matched by certificate designator
N52095 · ATA 7120

DURING INSPECTION OF ENGINE MOUNT AFTER ENGINE REMOVAL FOR OVERHAUL, CRACKS WERE FOUND AT BOTH FORWARD ENGINE MOUNTING BRACKET LOCATIONS. SUSPECT THAT CRACKS ARE DUE TO FATIGUE. CRACKS ARE DIFFICULT TO SEE WITH THE ENGINE INSTALLED DUE TO THE CLOSE PROXIMITY OF THE RUBBER MOUNTING PADS. RECOMMEND CLOSE INSPECTION OF THIS AREA AT ANNUAL INSPECTIONS.

Source: SDR 95ZZZX2947 · FAA SDRS

Linked aircraft

N-numberMake / modelYearStatusLink basis
N37362Matched by certificate designator
N5203XCESSNA TU206G1980Registration pendingMatched by certificate designator
N732DWCESSNA T210L1976Valid RegistrationMatched by certificate designator
N73TGMatched by certificate designator
N756YCCESSNA TU206G1978Valid RegistrationMatched by certificate designator
N9912QCESSNA 172M1975Valid RegistrationMatched by certificate designator