PINNACLE AIR CHARTER LLC
Also recorded as: PINNACLE AIR CHARTER, PINNACLE AIR CHARTER LLC, PINNACLE AVIATION, PINNACLE AVIATION CHARTER, Pinnacle Air Charter LLC
Accident & enforcement record
Events that happened, regardless of the operator's own reporting. Each links to its public source.
NTSB accidents & incidents
No NTSB accidents or incidents linked to this operator.
FAA enforcement actions
FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.
Maintenance disclosure history
Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.
12 reports on file.
RT ENGINE PYLON BLEED OVERHEAT, TROUBLE SHOT TO A LEAKING FLEX COUPLING ON HP BLEED DUCT.
INVESTIGATED REPORT OF RT (COPILOT'S) SIDE PITCH TRIM FAIL INDICATION. ALSO SHOWING RED "X" INDICATIONS FOR AIRSPEED, ALTITUDE, AND VERTICAL SPEED. ALTITUDE PRESELECT TURNS RED, THEN BLUE. REPLACED NR 2 AIR DATA COMPUTER WITH AN O/H UNIT, DISPLAY INDICATIONS NORMAL. RECOMMEND MFG SERVICE FACILITY INVESTIGATE AT TEAR-DOWN TO DETERMINE IF INTERNAL COMPONENT FAILURE OR WATER CONTAMINATION. SB 34-3972, MODIFICATION OF NR 2 AIR DATA COMPUTER PLUMBING, WAS PREVIOUSLY COMPLIED WITH.
INVESTIGATED REPORT OF FLIGHT MANAGEMENT SYS LOSING LAST SAVED POSITION, THEN GOING TO NORTH ZERO DEGREES AND EAST ZERO DEGREES. REPLACED NR 1 FMC-3000 FLIGHT MANAGEMENT COMPUTER CARD WITH AN O/H REPLACEMENT CARD AND RELOADED DATABASE. FMS OPS NORMAL. RECOMMEND MFG SERVICE FACILITY INVESTIGATE AT TEAR-DOWN TO DETERMINE IF CAUSED BY FAILED INTERNAL COMPONENT OR IF CAUSED BY WATER CONTAMINATION.
DURING SCHEDULED INSP, FOUND LT ENG COMPARTMENT FUEL HOSE ASSY CHAFED PAST SERVICE LIMITS FROM CONTACT WITH ADJACENT COWLING STRUCTURE. REPLACED HOSE ASSY WITH NEW HOSE ASSY AND SECURED AS REQUIRED. 390 SERIES POWERPLANT INSTALLATIONS HAVE TIGHT CLEARANCES BETWEEN HOSES, WIRING, TUBING, ETC. AND ADJACENT STRUCTURES, TECH SHOULD PAY CLOSE ATTENTION TO THE MM 71-00-00-201 INSP REQUIREMENTS WHENEVER LINES, TUBING, ETC. ARE DISTURBED. CLEARANCE INSP REQUIRED EACH 200 HR AIRFRAME INSP OR ENG INSTALLATION, SHOULD BE CLOSELY ADHERED TO.
DURING WHEEL DISASSEMBLY FOR TIRE REPLACEMENT FOUND WHEEL TIE BOLT CHAMFERED WASHERS INSTALLED INCORRECTLY, WITH CHAMFERED SIDES TOWARDS WHEEL HALF. NOTED WASHERS TO BE BENT, WHEEL TIE BOLT HEADS UNDERSIDE RADIUSES DAMAGED. SUSPECT TECHNICIAN ASSEMBLING WHEELS AT PREVIOUS TIRE CHANGE AT ANOTHER FACILITY DID NTO FULLY FOLLOW COMPONENT MM AND WAS NOT FAMILIAR WITH INSTALLATION OF MS20002 SERIES CHAMFERED WASHERS. (K)
DURING WHEEL DISASSEMBLY FOR TIRE REPLACEMENT FOUND WHEEL TIE BOLT CHAMFERED WASHERS INSTALLED INCORRECTLY, WITH CHAMFERED SIDES TOWARDS WHEEL HALF. NOTED WASHERS TO BE BENT, WHEEL TIE BOLT HEADS UNDERSIDE RADIUSES DAMAGED. SUSPECT TECHNICIAN ASSEMBLY WHEELS AT PREVIOUS TIRE CHANGE AT ANOTHER FACILITY DID NOT FULLY FOLLOW COMPONENT MM AND WAS NOT FAMILIAR WITH INSTALLATION OF MS20002 SERIES CHAMFERED WASHERS. (K)
DETECTED A RISE IN CABIN ALTITUDE THAT WAS NOT CONSIDERED NORMAL. MADE A PRECAUTIONARY DESCENT AND PERFORMED THE CABIN PRESSURE LOW CHECKLIST. LANDED AIRCRAFT AT INTENDED DESTINATION WITHOUT INCIDENT. FOUND A/C DISTRIBUTION DUCT FORWARD OF APU DISCONNECTED. RECONNECTED DUCT.
DURING ROUTINE OIL CHANGE METAL FOUND IN OIL FILTER. METAL FOUND TO BE BEARING MATERIAL COMING FROM CONNECTING ROD BEARING PREMATURE FAILURE. BEARING MATERIAL IS DELAMINATING. CONNECTING ROD BEARING MANUFACTURE DATES ARE (ML-KS 2-9A AND 3-99) MANUFACTURING DEFECT/PROBLEM KNOWN TO MFG. CRANKSHAFT GRIND REQUIRED TO CORRECT JOURNAL HEAT DEFECTS. (WPO1200303672)
WE ARE PERFORMING A PHASE A INSPECTION AGAIN 183.6 HOURS LATER. REMOVED ENGINE IGNITORS IN AN UNAIRWORTHY CONDITION. FOUND ALL FOUR IGNITORS IN AN UNAIRWORTHY CONDITION. THE CENTER ELECTRODE IS ABLE TO MOVE BACK AND FORTH INSIDE IGNITOR. TAKING THE IGNITOR IN HAND AND LIGHTLY SHAKING YOU CAN HEAR AND SEE CENTER ELECTRODE MOVING FORE AND AFT INSIDE IGNITOR BODY. FOLLOWING IS THE DATA FOUND ON THE IGNITOR BODY, ALL 4 IGNITOR S/N LISTED: (NR 1-99076345), NR 2-99076289, NR 3-99076330, NR 4-99076342.
WE ARE PERFORMING A PHASE A INSPECTION AGAIN 183.6 HOURS LATER. REMOVED ENGINE IGNITORS FROM BOTH ENGINES FOR INSPECTION ONLY. FOUND ALL FOUR IGNITORS IN AN UNAIRWORTHY CONDITION. THE CENTER ELECTRODE IS ABLE TO MOVE BACK AND FORTH INSIDE IGNITOR. TAKING THE IGNITOR IN HAND AND LIGHTLY SHAKING, YOU CAN HEAR AND SEE CENTER ELECTRODE MOVING FORE AND AFT INSIDE IGNITOR BODY . FOLLING IS THE DATA FOUND ON THE IGNITOR BODY, SN LISTED: NR 1-99076345, (NR 2-99076289), NR 3-99076330, NR 4-99076342.
WE ARE PERFORMING A PHASE A INSPECTION AGAIN 183.6 HOURS LATER. REMOVED ENGINE IGNITORS IN AN UNAIRWORTHY CONDITION. THE CENTER ELECTRODE IS ABLE TO MOVE BACK AND FORTH INSIDE IGNITOR. TAKING THE IGNITOR IN HAND AND LIGHTLY SHAKING YOU CAN HEAR AND SEE CENTER ELECTRODE MOVING FORE AND AFT INSIDE IGNITOR BODY. FOLLOWING IS THE DATA FOUND ON THE IGNITOR BODY, SN: NR1-99076345, NR2-99076289,( NR3-99076330), NR4-99076342.
WE ARE PERFORMING A PHASE A INSPECTION AGAIN 183.6 HOURS LATER. REMOVED ENGINE IGNITORS FROM BOTH ENGINES FOR INSPECTION ONLY. FOUND ALL FOUR IGNITORS IN AN UNAIRWORTHY CONDITION. THE CENTER ELECTRODE IS ABLE TO MOVE BACK AND FORTH INSIDE IGNITOR. TAKING THE IGNITOR IN HAND AND LIGHTLY SHAKING, YOU CAN HEAR AND SEE CENTER ELECTRODE MOVING FORE AND AFT INSIDE IGNITOR BODY. FOLLOWING IS THE DATA FOUND ON THE IGNITOR BODY, SN: NR1-99076345, NR2-99076289, NR3-99076330, (NR4-99076342)
Linked aircraft
| N-number | Make / model | Year | Status | Link basis |
|---|---|---|---|---|
| N196JH | CESSNA 525B | 2012 | Valid Registration | Matched by certificate designator |
| N205WA | ISRAEL AIRCRAFT INDUSTRIES GULFSTREAM 200 | 2005 | Valid Registration | Matched by certificate designator |
| N20BD | ISRAEL AIRCRAFT INDUSTRIES GULFSTREAM 200 | 2000 | Valid Registration | Matched by certificate designator |
| N20TW | CIRRUS DESIGN CORP SF50 | 2018 | Valid Registration | Matched by certificate designator |
| N365AV | BOMBARDIER INC BD-100-1A10 | 2017 | Valid Registration | Matched by certificate designator |
| N365LP | LEARJET INC 45 | — | Valid Registration | Matched by certificate designator |
| N390JV | — | — | Matched by certificate designator | |
| N3AS | BOMBARDIER INC BD-100-1A10 | 2024 | Valid Registration | Matched by certificate designator |
| N458WB | — | — | Matched by certificate designator | |
| N560TW | CESSNA 560XL | 2005 | Valid Registration | Matched by certificate designator |
| N611AV | BOMBARDIER INC BD-100-1A10 | 2017 | Valid Registration | Matched by certificate designator |
| N64VM | — | — | Matched by certificate designator | |
| N698RS | BOMBARDIER INC CL-600-2B16 | 2000 | Valid Registration | Matched by certificate designator |
| N763MT | BOMBARDIER AEROSPACE INC BD-100-1A10 | 2008 | Valid Registration | Matched by certificate designator |
| N823HM | LEARJET INC 45 | 2008 | Valid Registration | Matched by certificate designator |
| N895CC | BOMBARDIER INC CL-600-2B16 | 2007 | Valid Registration | Matched by certificate designator |
| N89CD | CIRRUS DESIGN CORP SR20 | 2005 | Valid Registration | Matched by certificate designator |
| N907WS | BOMBARDIER INC BD-700-1A11 | 2005 | Valid Registration | Matched by certificate designator |