RHOADES AVIATION INC.
Also recorded as: RHOADES AVIATION INC, RHOADES AVIATION INC., TRANSAIR
Accident & enforcement record
Events that happened, regardless of the operator's own reporting. Each links to its public source.
NTSB accidents & incidents
Operated by RHOADES AVIATION INC — Flag carrier (121), Supplemental Operator Does Business As: Transair (per NTSB report)
FAA enforcement actions
FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.
Maintenance disclosure history
Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.
96 reports on file — showing most recent 50.
CORROSION FOUND AT LH WING REAR SPAR LOWER CHORD UPPER HORIZONTAL FLANGE WBL 162
CRACK FOUND ON NO.5 FASTENER HOLE AT REAR SPAR UPPER CHORD OF LH WING AS MARKED. (STA RSS 222)
CRACK FOUND ON NO.5 FASTENER HOLE AT AFT SUPPORT FITTING AND REAR SPAR UPPER CHORD OF RH WING RSS 222
IN FLIGHT, CREW HAD WHEEL WELL OVERHEAT LIGHT AS WELL AS MASTER FIRE WARNING LIGHTS ILLUMINATE. LIGHTS EXTINGUISHED WHEN LANDING GEAR WAS EXTENDED. UPON LANDING, MAINTENANCE INSPECTION DETERMINED OVERHEAT SENSING LOOP CONNECTION WAS DIRTY, CLEANED AND PERFORMED OPERATIONAL CHECK PER AMM- 26-17-00. SYSTEM CHECKED NORMAL. NO FURTHER DEFECTS REPORT AFTER SUBSEQUENT FLIGHTS.
LONGITUDINAL FLOOR LONGITUDINAL FLOOR BEAM FOUND TWO CRACKS BETWEEN BS705 AND 715 RBL 24.82, CRACKS SIZE 3.0 INCH AND 1.5 INCH IN AREA.
CORROSION AT L/H WING SURGE TANK DRAIN VALVE (W STA 536)
CORROSION AT FWD UPPER R/H HORIZONTAL STABILIZER FRONT SPAR AT STAB. STA. 68~75
CORROSION AT FWD UPPER L/H HORIZONTAL STABILIZER FRONT SPAR AT STAB. STA. 68~79
EMER EXIT LIGHT BATTERY WEAK ON MAIN ENTRY DOOR UP SIDE. NRC:CA1251-01-014
ELT BATTERY TIME DUE ON 2021/JULY. NRC:CA1251-01-015
BULGE AT UPPER SKIN OF LH HORIZONTAL STABILIZER AT STAB. STA. 71~79 AND FROM REAR SPAR +1"
CORROSION AT LH SIDE THRUST BEAM UPPER SURFACE AT STA. 1105 ~ 1130. (5EA)
CORROSION AT L/H WING L/E FRONT SPAR LOWER CHORD HORIZONTAL LEG BETWEEN FSS 431 AND FSS 452
UPON APPLYING T/O THRUST NR 2 EPR GAUGE DID NOT RESPOND. T/O CLEARANCE CANCELLED, EXITED RUNWAY FOR TROUBLESHOOTING, NO RELIEF. CHECKED MEL, NO RELIEF, RETURNED TO RAMP.
CORROSION WAS FOUND AT LT WING BOTTOM SKIN LOWER SURFACE AT WS 475 TO WS 525.
CORROSION WAS FOUND AT AT LT WING BOTTOM SKIN LOWER SURFACE AT WS 315 TO WS 475.
EMERGENCY LIGHT INOPERABLE ON FWD ENTRY DOOR AND FWD GALLEY SERVICE DOOR.
EMERGENCY LIGHT INOPERABLE ON FWD ENTRY DOOR AND FWD GALLEY SERVICE DOOR.
CORROSION WAS FOUND AT LT WING BOTTOM SKIN LOWER SURFACE AT INBOARD TO WS 195.
CORROSION WAS FOUND AT AFT CARGO FWD BULKHEAD LOWER CHORD AT BS 727 BETWEEN S-25L AND 25R.
CORROSION WAS FOUND AT LT WING LEADING EDGE FRONT SPAR LOWER CHORD HORIZONTAL LEG AT FSS 135.
CORROSION WAS FOUND AT KEEL BEAM LOWER CHORD AT AFT CARGO BS 727 S-27L (LENGTH: 3" WIDTH: 1"). REFER TO NRC CA1174-02-010.
CORROSION WAS FOUND AT LT WING LEADING EDGE FRONT SPAR LOWER CHORD HORIZONTAL LEG AT FSS 307.
CORROSION WAS FOUND AT LT WING LEADING EDGE FRONT SPAR LOWER CHORD HORIZONTAL LEG AT FSS 422.
CORROSION WAS FOUND AT RT WING FRONT SPAR LOWER CHORD AT FSS 416.8.
CORROSION WAS FOUND AT RT WING FRONT SPAR LOWER CHORD AT FSS 442.3.
CORROSION WAS FOUND AT FWD & AFT SURFACE OF RT SIDE HORIZONTAL STABILIZER REAR SPAR UPPER LUG.
CORROSION WAS FOUND BETWEEN WING CENTER SECTION UPPER PANEL AND PRESSURE WEB SUPPORT ANGLE 65-82682-1 AT EACH BAY (FROM LBL 70 ~ RBL 70).
CORROSION WAS FOUND ON THRUST BEAM UPPER SURFACE AT HS CENTER SECTION STA. 1112.
CORROSION WAS FOUND ON LT WING LOWER SKIN UPPER SURFACE AT WS 155 NEAR FUEL BOOST PUMP ACCESS DOOR CUTOUT AREA.
CORROSION WAS FOUND ON LT WING LOWER SKIN TRAILING EDGE AREA AT WS 450.
CORROSION WAS FOUND ON MAIN CARGO DOOR BODY UPPER SILL.
PILOT OBSERVED #2 ENGINE LOW OIL PRESSURE LIGHT IN FLIGHT AND PERFORMED IN FLIGHT SHUT DOWN PROCEDURES
NR 1 ENGINE FAIL AT AROUND 2000FT. ON FINAL PERFORMED ENGINE FAILURE/SHUTDOWN CHECKLIST (QRH).
NUMBER 2 ENGINE FIRE LIGHT CAME ON IN FLIGHT. MX DISCOVERED BROKEN NUMBER 2 ENGINE FIRE DETECTOR LOOP CONNECTOR. ITEM PREVIOUSLY MEL'D PER MEL 737071618-1. PERFORMED SYSTEM OPS CHECKS PER AMM 26-11-00. OPS CHECK GOOD.
LEFT HAND FWD EMERGENCY EXIT LIGHT INOP. REMOVED AND REPLACED EXIT LIGHT AND OPS CHECK GOOD IAW AMM 33-51-02.
NR 1 ENGINE FAILED DURING TAKEOFF, GOT 3 BACK FIRING BEFORE ENGINE SHUTDOWN, QRH COMPLETED. REMOVED FUEL PUMP AND DISCOVERED IT HAD A BROKEN SHAFT. INSTALLED NEW FUEL PER MM 72-00-61 AND OPS CHECKED IT PER AMM 71-09-100.
IN FLIGHT, SMOKE IN COCKPIT WITH STRONG SMELL OF ELECTRICAL BURNING. EMERGENCY DECLARED, REQUESTED RETURN TO AIRPORT. COMPLIED WITH QRH. CAPTAIN PUT ON QUICK DOM OXYGEN MASK. SMOKE DISSIPATED AFTER 1 MINUTE. FOUND AIR GASPER FAN CIRCUIT BREAKER POPPED OPEN UPON INSPECTION ON POST FLIGHT. AIRCRAFT IS CURRENTLY IN SERVICE FLYING UNDER RAI MEL NR 306040517-1 REF 21-24 CAT D DUE DATE: 08/03/2017. THE DEFECTIVE PART (GASPER FAN) S/N WILL BE ESTABLISHED UPON REMOVAL. REPLACEMENT PART ON ORDER.
DURING A C1 CHECK, FOUND THE LEFT WING UPPER SURFACE WAS CORRODED ON REAR SPAR BETWEEN WS 150 - 205. CORROSION WAS BLENDED OUT BEYOND SRM LIMIT. REPAIRED IAW DOCUMENT ROO3 REV 01.
DURING INSPECTION IAW CARD 53-30-00-101, FOUND FUSELAGE SKIN AT BS 1016 BETWEEN STRINGERS 24R - 25R WAS CORRODED. A REPAIR WAS CARRIED OUT IAW DOCUMENT 2016R002.
COCKPIT L2 WINDOW CRACKED. APPEARS HEATING ELEMENT SHORTED, CRACKED OUTER PANE DETERMINED NON STRUCTURAL, FLIGHT CONTINUED, LANDED WINDOW INSPECTED AND ACFT RETURNED TO HOME BASE UNDER SPECIAL FERRY PERMIT. RESTRICTIONS, UNPRESSURIZED, BELOW 10,000FT. UNIT WAS A USED INSPECTED SERVICEABLE ITEM OF UNKNOWN LIFE AND HISTORY. INSPECTED AND SIGNED FOR, PERFORMED 42 PROCEDURES AT INSTALL, PASSED ALL INSPECTIONS AND RESISTANCE TESTING, OPERATED SUCCESSFULLY FROM 4/19/2016, FAILED THIS DAY 5/25/2016.
UNCOMMANDED LT MLG EXTENSION IN FLIGHT AT 315 KNOTS. REDUCED AIRSPEED AND REDUCED ALTITUDE. CORRECTED SEVERE YAW. SELECTED GEAR DOWN, 3 DOWN & LOCKED. CONTINUE TO DESTINATION. FLY-BY CONFIRMED GEARS DOWN AND PERFORMED A SAFE LANDING. JACKED ACFT, AND TROUBLESHOOT TO FAULTY INTERNALS, TIGHT ACTUATING PISTON IN MLG SELECTOR VALVE. REPLACED LANDING GEAR SELECTOR VALVE, GEAR SWUNG MULTIPLE TIMES, COULD NOT DUPLICATE MAIN GEAR UNCOMMANDED EXTENSION. SERVICED HYDRAULICS AND RETURNED ACFT TO SERVICE.
COCKPIT L2 SLIDING WINDOW CRACKED. APPEARS HEATING ELEMENT SHORTED, CRACKED OUTER PANE DETERMINED NONSTRUCTURAL, FLIGHT CONTINUED & LANDED. WINDOW INSPECTED, ACFT RETURNED TO HOME BASE ON SPECIAL FERRY FLIGHT PERMIT, ISSUED 4 19 2016. REPLACEMENT WINDOW INSTALLED. NOTE TOTAL TIME & CYCLES UNKNOWN, 10000 HRS & CYCLES USED ONLY FOR COMPLETION OF THIS SDR.
RIGHT FUEL TANK DUMPING FUEL INTO CTR TANK IN FLIGHT. TURNED ON CTR TANK RT BOOST PUMP & TURNED OFF RT TANK FUEL PUMPS. LANDED WITH 5400 LBS LT TANK, 4000 LBS RT TANK & 2000 LBS IN CTR TANK. FLIGHT BEGAN WITH 16000 LBS FUEL ON BOARD & CTR TANK ALMOST EMPTY. CARGO FLIGHTS ARE OF 30 MINS DURATION & CTR FUEL TANK ALMOST NEVER USED AT ALL. ACFT TURNED AROUND & LANDED BACK AT AIRPORT. TOTAL FLIGHT TIME 0.6 HRS, BLOCK 8. REPLACED CTR TANK ON WAY FUEL CHECK VLV. FLAPPER RETURN SPRING WAS BROKEN, TOP & BOTTOM FLAPPERS REMAINED OPEN ALLOWING FUEL MIGRATION BACK INTO CTR TANK FROM RT WING TANK. FUEL MIGRATION ISSUES NOW RESOLVED.
INSPECTION FOUND LT KEEL BEAM LOWER CHORD, LBBL 6.30, CORRODED BETWEEN BS 540-BS 580. THE CORRODED HORIZONTAL FLANGE SECTION WAS BLENDED AND TRIMMED OUT. INSTALLED REPAIR FILLERS, REPAIR STRAP AND REPAIR ANGLE IAW REPAIR PLAN 121083-R041, REV 02.
INSPECTION FOUND LT KEEL BEAM LOWER CHORD, LBL 6.30, CORRODED AND CRACKED BETWEEN BS 668 - 672. THE KEEL BEAM LOWER CHORD WAS CUT AT BS 625 AND THE KEEL BEAM AFT SEGMENT WAS REMOVED AND THEN REPLACED WITH NEW PART BETWEEN BS 625-BS 727+16 IAW REPAIR PLAN NR 121083-R041, REV 02.
INSPECTION FOUND CENTER TANK LOWER SKIN CORRODED BETWEEN S-4C TO S-5C, LBBL 6.30 TO RBBL 6.30. THE CORRODED SKIN AREAS WERE BLENDED. THE AREA WAS FOUND OUT OF SRM ALLOWABLE LIMIT AND REPAIRED IAW REPAIR PLAN 121083-R043, REV 06.
INSPECTION FOUND STRINGER FITTING AT STRINGER 27R, BS 1016 BULKHEAD CORRODED. THE DAMAGED STR FITTING WAS R & R BY INSTALLING A NEW FITTING IAW SRM 51-3-02, REV 108.
INSPECTION FOUND CENTER TANK LOWER SKIN CORRODED BETWEEN S-9C TO S-10C, LBBL 6.30 TO RBBL 6.30. THE CORRODED SKIN AREAS WERE BLENDED. THE AREA WAS FOUND OUT OF SRM ALLOWABLE LIMIT AND REPAIRED IAW REPAIR PLAN 121083-R043, REV 06. EXTERNAL REPAIR DOUBLER WAS INSTALLED UNDER SKIN PANEL FOR BLEND OUT AREA BETWEEN S-9C TO S-10C.
INSPECTION FOUND STRINGER FITTING AT S-25R, STA 1016 BULKHEAD CORRODED. THE DAMAGED STRINGER FITTING WAS R & R BY INSTALLING A NEW FITTING IAW SRM 51-3-02, REV 108.
Linked aircraft
| N-number | Make / model | Year | Status | Link basis |
|---|---|---|---|---|
| N810TA | BOEING 737-275C | 1975 | Valid Registration | Operator named in NTSB report |