OMNI AIR TRANSPORT, LLC

Part 135 operator · designator O2MA

Data confidence: All records on this page are linked by a shared certificate number or aircraft registration (N-number).

Also recorded as: OMNI AIR TRANSPORT, LLC

Accident & enforcement record

Events that happened, regardless of the operator's own reporting. Each links to its public source.

NTSB accidents & incidents

No NTSB accidents or incidents linked to this operator.

FAA enforcement actions

FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.

Maintenance disclosure history

Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.

14 reports on file.

O · 2023-04-18 Matched by certificate designator
N340SR · ATA 8000

SWITCH GUARDS LOCATED ON THE CENTER PEDESTAL DO NOT FUNCTION WELL. A MAIN ENGINE START SWITCH GUARD WAS FOUND PUSHED TO THE SIDE AND PRESSED/JAMMED INTO THE SWITCH CAUSING UNCOMMANDED ACTIVATION WITHOUT LIFTING THE GUARD AND PRESSING THE SWITCH. ANOTHER AIRCRAFT, ALSO LEAR 45, A MAIN ENGINE FIRE EXTINGUISHER SWITCH GUARD WAS FOUND TO PRESS INTO THE SWITCH WHEN THE GUARD WAS NOT ALIGNED CAUSING INADVERTENT ACTIVATION WITHOUT LIFTING THE GUARD AND PRESSING THE SWITCH.

Source: SDR JGVR20230518001 · FAA SDRS
O · 2021-05-23 Matched by certificate designator
N340SR · ATA 5610

DURING DESCENT THROUGH ABOUT 10,000' A LOUD POP WAS HEARD AND RH WINDSHIELD WAS SEEN TO HAVE SHATTERED. NO PRESSURIZATION WAS LOST, CREW FOLLOWED QRH AND CONTINUED NORMAL PROCEDURES AND LANDED WITHOUT INCIDENT. UPON LANDING IT WAS DISCOVERED THAT THE OUTER PLY OF WINDSHIELD HAD SHATTERED. NO OTHER DAMAGE TO THE AIRCRAFT AND NO INJURIES NOTED.

Source: SDR O2MA4520430292 · FAA SDRS
O · 2021-03-31 Matched by certificate designator
N340SR · ATA 5610

DURING CLIMB AROUND FL290 LOUD POPPING SOUND WAS HEARD AND RH WINDSHIELD WAS OBSERVED TO BE CRACKED. CREW ANALYZED SITUATION, STOPPED CLIMB, FOLLOWED THE QRH AND DIVERTED BACK TO AIRPORT. UPON LANDING OUTER PLY OF WINDSHIELD WAS FOUND TO BE SHATTERED. NO OTHER DAMAGE NOTED AND NO INJURIES.

Source: SDR O2MA4520430269 · FAA SDRS
O · 2020-06-07 Matched by certificate designator
N340SR · ATA 2130

ON CLIMB-OUT, ENROUTE, CREW HEARD A POPPING SOUND FROM THE LEFT SIDE OF THE AIRCRAFT AS THE AIRCRAFT PASSED FL320. NO AIR WAS FELT COMMING FROM THE VENTS. CREW DONNED OXYGEN MASKS WHEN THEY NOTED CABIN ALTITUDE APPROACHING CLIMBING TOWARD 10,000 FT. EMERGENCY DESCENT WAS INITIATED AND EMERGENCY WAS DECLARED. AIRCRAFT DIVERTED.

Source: SDR KW3R20200607240 · FAA SDRS
O · 2018-03-15 Matched by certificate designator
N21AX · ATA 5200

AFTER LANDING, DISCOVERED A FUELING DOOR OPENED IN FLIGHT AND DAMAGED DOOR AND HINGE.

Source: SDR O2MA2018F00139 · FAA SDRS
O · 2018-03-14 Matched by certificate designator
N21AX · ATA 5246

ON LANDING, DISCOVERED FUELING DOOR OPENED IN FLIGHT AND DAMAGED THE DOOR AND HINGE.

Source: SDR O2MA180314 45551 · FAA SDRS
R · 2016-08-17 Matched by certificate designator
N360AX · ATA 7603

AFTER START UP OF ENGINES, ACFT BEGAN TO TAXI AND THE PILOT REPORTED RT THROTTLE LEVER BECAME UNRESPONSIVE DURING TAXI. THEY RETURNED AND AFTER TROUBLESHOOTING IT WAS DETERMINED THE CONTROL ASSY, PN 7-43489-2, FOR THE RT ENGINE HAD SHEARED IN HALF, 6" FROM THE END AT THE ENGINE SIDE CONNECTION.

Source: SDR O2MA2016F00173 · FAA SDRS
O · 2016-08-09 Matched by certificate designator
N45KH · ATA 5610

DURING CRUISE AT 41,000 FEET, THE RIGHT WINDOW DELAMINATED RESULTING IN AN EMERGENCY DECENT AND LANDING AT THE CLOSEST AIRPORT.

Source: SDR 2016F00165 · FAA SDRS
X · 2012-02-07 Matched by certificate designator
N72AX · ATA 7314

DURING THE APPROACH THE LT ENGINE FLAMED OUT WHEN THE THROTTLE LEVER WAS RETARDED TOWARDS FLIGHT IDLE. THE PIC DECLARED AN EMERGENCY AND THE AIRCRAFT LANDED WITH NO INCIDENT. THE LT ENGINE WAS NEVER ATTEMPTED TO BE RESTARTED DURING THE APPROACH. ATTEMPTS WERE MADE AT STARTING THE ENGINE WITH NO SUCCESS AND THE FUEL FLOW WAS NOTICED TO BE READING ZERO. MAINTENANCE INSTALLED A PRESSURE GAUGE DIRECTLY TO THE LT ENGINE FUEL PUMP AND DURING A START ATTEMPT FOUND THE PUMP TO BE PRODUCING 0 PSI. THE PUMP WAS REMOVED AND THE IMPELLER WITHIN THE PUMP WAS FOUND TO BE NOT FUNCTIONING. A NEW PUMP WAS ORDERED AND IS BEING INSTALLED AS OF 1500 ON 2/8/12.

Source: SDR O2MA20120207001 · FAA SDRS
X · 2012-01-27 Matched by certificate designator
N72AX · ATA 7603

SHORTLY AFTER THROTTLING BACK TO FLIGHT IDLE TO DESCEND FROM 41,000 FT THE NR 2 ENGINE MOMENTARILY STAYED AT 80 PERCENT (APPROXIMATELY 15 SECONDS) AND THEN CONTINUED ROLLING DOWN AND FLAMED OUT. PILOT WINDMILL RESTARTED THE ENGINE AT APPROXIMATELY 26,000 FT AND HAD TO RESET THE FUEL COMPUTER TO TURN OFF THE COMPUTER LIGHT. SLIGHT ENGINE SURGE WHICH CREATED A SLIGHT YAW WAS NOTICED AT 6,000 FT. ONCE ON THE GROUND WITH THE ENGINES SHUT OFF THE NR 2 ENGINE FUEL COMPUTER LIGHT WAS REPORTED AS FLASHING. MAINTENANCE DISPATCHED TO THE AIRCRAFT WITH A LAPTOP AND UPON DOWNLOAD FOUND THE N2 MONOPOLE HAD CAUSED A FAULT WHICH WAS PICKED UP BY THE DEEC. A NEW N2 MONOPOLE WAS INSTALLED AND THE ENGINE WAS RAN WITH NO FURTHER PROBLEMS NOTED AND THE DEEC WAS CHECKED WITH NO FURTHER FAULT CODES FOUND.

Source: SDR O2MA20120127001 · FAA SDRS
N · 2011-06-21 Matched by certificate designator
N360AX · ATA 2612

DURING CLIMB TO ALTITUDE THE RT ENGINE FIRE LIGHT ILLUMINATED MOMENTARILY. THROTTLE LEVER WAS RETARDED MOMENTARILY BUT LIGHT WENT OUT WITH NO OTHER INDICATIONS OR WARNINGS. AIRCRAFT FIRE DETECTION SYSTEM CURRENTLY BEING INVESTIGATED FOR CAUSE OF MOMENTARY LIGHT.

Source: SDR O2MAN36062111 · FAA SDRS
G S J · 2011-03-09 Matched by certificate designator
N27AX · ATA 2420

AUTOPILOT FAILED AT CRUISE FOLLOWED BY PRIMARY PITCH TRIM FAIL, MACH TRIM FAIL, DURING DESCENT AC BUSS TIE C/B POPPED. AMMETERS INDICATED 50 AMP DIFFERENCE. DURING TROUBLESHOOTING OF THE AUTOPILOT, PITCH TRIM, MACH TRIM & AC BUSS SYSTEMS FOUND CONNECTOR P213 FOR AC PARALLELING BOX TO NOT BE FULLY SECURED. RESECURED P213 AND PERFORMED NUMEROUS OPS CHECKS OF AUTOPILOT, PITCH TRIM, MACH TRIM & AC SYSTEMS WITH NO DEFECTS NOTED AT THIS TIME. IAW AMM CH 22-10, 27-41, AND 24-20. PERFORMED ADJUSTMENT TO THE RT VOLTAGE REGULATOR FOR THE RT GEN AMP SPLIT IS WITHIN LIMITS DURING ALL VARIOUS LOADS IAW AMM 24-31-03.

Source: SDR 2011FA0000173 · FAA SDRS
N · 2007-02-26 Matched by certificate designator
N45AX · ATA 2620

FIRE BOTTLE GAUGE HAS INACCURATE INDICATION, FOUND TO INDICATE (0) ON PREFLIGHT. THE BOTTLE WAS REMOVED AND DETERMINED TO BE FULL OF AGENT AND NOTICED ROTATING THE BOTTLE MOVED THE PRESSURE GAUGE. BY HAND SHAKING THE BOTTLE THE PRESSURE INDICATION WOULD MOVE FROM A (0) INDICATION UP TO 800 PSI. THE BOTTLE WAS REPLACED WITH AN O/H UNIT.

Source: SDR 45AX022607 · FAA SDRS
O · 2000-10-31 Matched by certificate designator
N453 · ATA 3010

LEFT HORIZONTAL STABLILIZER HEAT BLANKET SHEARED, BURNING A .6250 INCH HOLE IN THE LEADING EDGE OF THE HORIZONTAL STABILIZER 5 INCHES OUTBOARD FROM THE INBOARD EDGE. (X)

Source: SDR 20001129SH015 · FAA SDRS

Linked aircraft

N-numberMake / modelYearStatusLink basis
N18AXLEARJET INC 45Valid RegistrationMatched by certificate designator
N21AXMatched by certificate designator
N33WLLEARJET INC 602006Valid RegistrationMatched by certificate designator
N340SRLEARJET INC 452006Valid RegistrationMatched by certificate designator
N45AXMatched by certificate designator
N45KHLEARJET INC 452006Valid RegistrationMatched by certificate designator
N75SRLEARJET INC 45Valid RegistrationMatched by certificate designator
N784APHAWKER BEECHCRAFT CORP B3002011Valid RegistrationMatched by certificate designator