Air MD L.L.C.

Part 135 operator · designator YEWA

Data confidence: Records are linked by certificate number, aircraft registration, or a name match that a reviewer has confirmed. Each record below shows how it was linked.

Also recorded as: AIR MD LLC, Air MD L.L.C.

Accident & enforcement record

Events that happened, regardless of the operator's own reporting. Each links to its public source.

NTSB accidents & incidents

Acc · 2011-05-26 Operator named in NTSB report
BELL 206 (N1815) Minor injury Part 91

Operated by AIR MD LLC (per NTSB report)

Source: NTSB case CEN11LA356
Accident · 1984-09-07 Matched by aircraft (N-number)
Cessna T210M (N191WB) Fatal injury
Source: NTSB case SEA84FA223

FAA enforcement actions

FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.

Maintenance disclosure history

Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.

11 reports on file.

F · 2021-06-30 Matched by certificate designator
N911ZC · ATA 5753

DURING FINAL APPROACH, THE LH OTBD FLAP I/B FLAP TRACK BROKE INTO TWO PIECES ALLOWING THE FLAP TO CANT CAUSING IT TO JAM AND NOT ALLOW TRAVEL TO THE APPROACH POSITION. BECAUSE THE FLAP WAS CANTED IT ALSO ALLOWED IT TO CONTACT THE LH AILERON INDUCING A RESISTANCE IN THE YOKE IN A SMALL RANGE OF MOVEMENT OF THE AILERONS. THE LIMITED EXTENSION OF THE LH OTBD FLAP ALSO INDUCED A CONTROLLABLE A-SYMMETRIC LIFT CONDITION.AIRCRAFT LANDED SAFELY AND PROCEEDED TO PARKING.

Source: SDR YEWA2021F00072 · FAA SDRS
R · 2020-08-31 Matched by certificate designator
N813JB · ATA 7810

PILOT REPORTED HEARING A POP UPON ADVANCING PROP LEVERS ON MID-FINAL APPROACH INTO KAAO. PILOT NOTICED NR 1 ENGINE TORQUE INDICATION EXTREMELY LOW, LANDING WAS COMPLETED PER NORMAL PROCEDURES WITHOUT INCIDENT. VISUAL INSPECTION OF THE NR 1 ENGINE FOUND THE POWER SECTION INNER EXHAUST LINER HAD TORN AND MADE CONTACT WITH THE POWER TURBINE DISC. THE POWER SECTION WAS REMOVED AND SENT TO CTS FOR REPAIR. CTS DETERMINED THE CAUSE FOR PT BLADE FAILURE WAS RELATED TO EXHAUST BEARING SUPPORT COVER FAILURE. THE NR 3 BEARING COVER & SKI JUMP (EXHAUST DUCT) CRACKED AND EVENTUALLY CONTACTED PT BLADES CAUSING THE BLADES TO FAIL.

Source: SDR YEWA20200910002 · FAA SDRS
O · 2020-08-12 Matched by certificate designator
N925MD · ATA 2434

DURING SCHEDULED INSPECTION OF STARTER/GENERATOR, WE FOUND A MOLTEN HOLE IN THE FAN COVER AT THE REAR OF THE GENERATOR. UPON REMOVING THE COVER, WE FOUND ONE OF THE BRUSH LEADS HAD SHORTED TO THE CASE, DAMAGING THE CASE AND THE LEAD. IT WAS ALSO NOTICED THAT ADJACENT TO SOME BRUSH LEADS THERE WAS AN ANTI-CHAFE/INSULATING TAPE APPLIED TO THE COVER, BUT NOT AT THIS LOCATION. THERE WAS NO INSULATION ON ANY OF THE BRUSH LEADS. WHEN WE INSPECTED TWO OTHER GENERATORS, WE FOUND NO INSULATION TAPE, BUT ALL OF THE BRUSH LEADS WERE INSULATED WITH A "SNAKE SKIN". WE CONTACTED PRECISION HELIPARTS LOUISIANA, WHO HAD DONE THE LAST OVERHAUL. THEY TOLD US THERE HAD BEEN A HISTORY OF THE THESE GENERATORS HAVING THE INSULATING TAPE COME LOOSE FROM THE COVER AND INGESTING IT, LEAVING THE BRUSH LEAD UNPROTECTED AND THERE WAS A NEW LEAD AVAILABLE THAT WAS INSULATED AND DIDN'T NEED THE INSULATING TAPE.

Source: SDR YEWA20200910001 · FAA SDRS
O · 2020-08-04 Matched by certificate designator
N997MD · ATA 2750

FLAP ROLLER BRACKETS IN FLAPS CHAFED BY FLAP BEARINGS REQUIRING REPLACEMENT. (R/H INBD FLAP, INBD TRACK, OTBD BRACKET P/N 50-160003-5)(R/H OTBD FLAP, INBD TRACK, OTBD BRACKET P/N 35-165050-31)(R/H OTBD FLAP, OTBD TRACK, INBD BRACKET P/N 35-165050-34)(L/H INBD FLAP,INBD TRACK, OTBD BRACKET P/N 50-160003-4).

Source: SDR YEWA2020080501 · FAA SDRS
F · 2020-05-26 Matched by certificate designator
N911ZC · ATA 5753

DURING FLIGHT, THE NR 4 FLAP I/B FLAP TRACK BROKE INTO TWO PIECES ALLOWING THE FLAP TO CANT CAUSING IT TO JAM AND NOT ALLOW TRAVEL TO THE APPROACH POSITION. BECAUSE THE FLAP WAS CANTED IT ALSO ALLOWED IT TO CONTACT THE RT AILERON INDUCING A RESISTANCE IN THE YOKE IN A SMALL RANGE OF MOVEMENT OF THE AILERONS. THE LIMITED EXTENSION OF THE NR 4 FLAP ALSO INDUCED A CONTROLLABLE A-SYMMETRIC LIFT CONDITION.

Source: SDR YEWA20200630001 · FAA SDRS
O · 2020-03-25 Matched by certificate designator
N771PA · ATA 2750

MULTIPLE FLAP ROLLER BRACKETS INSIDE FLAPS CHAFED BY FLAP ROLLERS REQUIRING REPLACEMENT. (L/H OTBD FLAP, OTBD TRACK, INBD BRACKET P/N 35-165050-35)(L/H OTBD FLAP, INBD TRACK, INBD AND OTBD BRACKETS P/N 35-165050-31, P/N 35-165050-30)(L/H INBD FLAP, INBD TRACK, OTBD BRACKET P/N 50-160003-4)(R/H INBD FLAP, INBD TRACK, INBD AND OTBD BRACKETS P/N 50-160003-5, P/N 50-160003-4)(R/H OTBD FLAP, OTBD TRACK, INBD BRACKET P/N 35-165050-35)(R/H OTBD FLAP, INBD TRACK, OTBD BRACKET P/N 35-165050-31).

Source: SDR YEWA20200806001 · FAA SDRS
O · 2020-03-11 Matched by certificate designator
N191WB · ATA 2750

MULTIPLE FLAP ROLLER BRACKETS INSIDE FLAPS WERE CHAFED BY THE FLAP ROLLERS REQUIRING REPLACEMENT.

Source: SDR YEWA20200806002 · FAA SDRS
O · 2020-02-19 Matched by certificate designator
N813JB · ATA 2750

MULTIPLE FLAP ROLLER BRACKETS INSIDE FLAPS CHAFED BY FLAP ROLLERS REQUIRING REPLACEMENT. (R/H INBD FLAP,INBD TRACK, OTBD BRACKET P/N 50-160003-5)(L/H OTBD FLAP, OTBD TRACK, INBD AND OTBD BRACKETS P/N 35-165050-30 P/N 35-165050-35)

Source: SDR YEWA20200806003 · FAA SDRS
O · 2016-06-01 Matched by certificate designator
N5751M · ATA 5302

PERFORMED ASB206L-09-158B UPPER LT TAILBOOM FITTING INSPECTION. FOUND UPPER LT TAILBOOM FITTING, PN 206-032-409-001 CRACKED. R & R FITTING WITH NEW.

Source: SDR YEWA201606240001 · FAA SDRS
B · 2015-07-17 Matched by certificate designator
N969MA · ATA 2121

AFTER TAKE OFF, PASSING THROUGH 16,000 FEET, OBSERVED AND SMELLED SMOKE IN THE AIRCRAFT. IT APPEARED TO ME TO BE VERY LIGHT GREY SMOKE, AND HAD AN ACRID SMELL AND WAS SLIGHTLY IRRITATING TO THE EYES AND THROAT. THE MED CREW IN THE REAR SAID THEY COULD ALSO SEE AND SMELL THE SMOKE. WE IMMEDIATELY REQUESTED AND RECEIVED CLEARANCE TO RETURN TO THE DEPARTURE AIRPORT AND LANDED PROMPTLY AND SAFELY WITHOUT ANY INCIDENT. NO EMERGENCY SERVICES WERE REQUIRED NOR REQUESTED. ON THE GROUND A LOCAL MECHANIC WAS LOCATED. WORKED WITH LIFETEAM MAINTENANCE, PERFORMED GROUND OPERATION CHECKS AND COULD NOT DUPLICATE. DID LOCAL AREA TEST FLIGHT. COULD NOT DUPLICATE. AIRCRAFT WAS TAKEN TO NEWTON FOR RE-INSPECTION. LIFETEAM FOUND THE FWD VENT BLOWER HAD FAILED. BLOWER HAS BEEN REPLACED AND AIRCRAFT RETURNED TO SERVICE. NO RECORD OF INSTALLATION WAS FOUND. COULD HAVE BEEN INSTALLED BY THE FACTORY.

Source: SDR 2015FA0000326 · FAA SDRS
O · 2004-09-07 Matched by certificate designator
N77HE · ATA 3246

INNER WHEEL HALF OF WHEEL ASSEMBLY PN 40-170A, SN 10, HEAT LOT NR 283 WAS REJECTED DURING EDDY CURRENT INSPECTION FOR CRACKS IN EXCESS OF 0.010 INCH. INDICATIONS WERE FOUND IN THE AREA OF BEAD SEAT OF THE INNER HALF OF THE WHEEL ASSEMBLY ONLY, NO INDICATIONS WERE FOUND ON THE OUTER WHEEL HALF OF THE ASSEMBLY.

Source: SDR 2004FA0000735 · FAA SDRS

Linked aircraft

N-numberMake / modelYearStatusLink basis
N1815Operator named in NTSB report
N191WBMatched by certificate designator
N771PABEECH C901983Valid RegistrationMatched by certificate designator
N77HEBEECH C901981Valid RegistrationMatched by certificate designator
N813JBBEECH C901980Valid RegistrationMatched by certificate designator
N911ZCRAYTHEON AIRCRAFT COMPANY C90AValid RegistrationMatched by certificate designator
N911ZEBEECH C90AValid RegistrationMatched by certificate designator
N969MABEECH 2001981Valid RegistrationMatched by certificate designator