SUBURBAN AIR FREIGHT, INC.

Part 135 operator · designator JDWA

Data confidence: All records on this page are linked by a shared certificate number or aircraft registration (N-number).

Also recorded as: SUBURBAN AIR FREIGHT, INC., Suburban Air Freight, Inc.

Accident & enforcement record

Events that happened, regardless of the operator's own reporting. Each links to its public source.

NTSB accidents & incidents

No NTSB accidents or incidents linked to this operator.

FAA enforcement actions

FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.

Maintenance disclosure history

Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.

19 reports on file.

R · 2018-04-17 Matched by certificate designator
N130UE · ATA 7321

DURING APPROACH, THE NR 1 POWER OUTPUT REDUCED AND WOULD NOT RESPOND TO INPUT. THE ENGINE WAS SHUT DOWN AND AIRCRAFT LANDED WITHOUT INCIDENT. TROUBLESHOOTING REVEALED NO DAMAGED P3 OR PY LINES. REPLACED FUEL CONTROL UNIT.

Source: SDR JDWA201804190001 · FAA SDRS
D · 2016-10-28 Matched by certificate designator
N124GP · ATA 5610

A PORTION OF THE COPILOT SIDE WINDOW DEPARTED THE AIRCRAFT DURING CLIMB AT 15,000 FT. AIRCRAFT RETURNED TO DEPARTURE AIRPORT. UPON INSPECTION, THE AIRFRAME STRUCTURE AND WINDOW FLANGE WERE NOT DAMAGED. THE REMNANTS OF THE EXISTING WINDOW WERE REMOVED, AND A NEW WINDOW WAS INSTALLED IN ACCORDANCE WITH THE MANUFACTURERS MAINTENANCE MANUAL.

Source: SDR 2016F00213 · FAA SDRS
O · 2012-11-15 Matched by certificate designator
N719GL · ATA 2340

PILOT'S MICROPHONE BUTTON STUCK. PILOT RETURN TO DEPARTURE. MX REPLACED MIC BUTTON.

Source: SDR JDWA719GL002 · FAA SDRS
F · 2011-07-18 Matched by certificate designator
N864SF · ATA 2731

ELEVATOR TRIM STIFF.

Source: SDR JDWA864SF001 · FAA SDRS
N · 2010-10-26 Matched by certificate designator
N147SF · ATA 5270

ON TAKEOFF ROLL, CABIN DOOR LIGHT CAME ON BEFORE LIFTOFF. PILOT ABORTED TAKEOFF AND WENT BACK TO RUN UP PAD. CHECKED DOOR AND TRIED ANOTHER TAKEOFF, DOOR LIGHT CAME ON BEFORE ACFT LT THE GROUND. RETURNED TO RAMP, MECHANIC RESET DOOR LIGHT SWITCH. SYS FUNCTION CHECKED SATISFACTORY.

Source: SDR JDWA147SF1 · FAA SDRS
J · 2010-09-07 Matched by certificate designator
N147SF · ATA 3230

AFTER TAKEOFF, THE GEAR IN-TRANSIT LIGHT CAME ON. PILOT RETURNED WITHOUT FURTHER INCIDENT.

Source: SDR JDWA147F1 · FAA SDRS
J · 2010-08-25 Matched by certificate designator
N128SF · ATA 3150

AFTER TAKEOFF, THE HYD LIGHT CAME ON AND STAYED ON. PILOT RETURNED WITHOUT FURTHER INCIDENT.

Source: SDR 2010FA0000894 · FAA SDRS
N · 2009-11-27 Matched by certificate designator
N118SF · ATA 3297

ON APPROACH, NO NOSE GEAR DOWN LOCK LIGHT. PILOT CHECKED THE DOWN POSITION BY OPERATING HANDPUMP. LANDED WITHOUT INCIDENT. MECHANIC CALLED OUT, WIRE FROM THE DOWNLOCK SWITCH (PN 1CH25) WAS FOUND TO BE BROKEN. WIRE WAS REPAIRED, SYS OPS CHECK WAS OKAY. PLANE DEPARTED THE FOLLOWING DAY WITHOUT FURTHER INCIDENT.

Source: SDR JDWA118SF2 · FAA SDRS
J · 2009-08-07 Matched by certificate designator
N719GL · ATA 7261

AFTER TAKEOFF DURING CLIMB, PILOT NOTICED RT OIL PRESSURE ANNUNCIATOR LIGHT AND NOTED OIL PSI TO BE 50PSI. PILOT REDUCED PWR AND RETURNED TO BASE WITHOUT INCIDENT.

Source: SDR JDWA31764A · FAA SDRS
N · 2009-04-21 Matched by certificate designator
N7994R · ATA 2612

UPON TAKEOFF ROLL, THE RT FIRE LIGHT CAME ON. PILOT IMMEDIATELY REDUCED POWER AND ABORTED TAKEOFF RUN. LIGHT WENT OUT ENROUTE BACK TO MX FACILITY. NO FIRE OR SMOKE WAS FOUND.

Source: SDR JDWA7994R · FAA SDRS
R · 2009-01-26 Matched by certificate designator
N118SF · ATA 6120

ON CLIMB OUT, LEFT PROPELLER RPM DROPPED FROM 2200 TO 1900 RPM. PILOT TOOK NOTE AND CALLED IN FOR RETURN. MAINTENANCE HAS NOT DETERMINED THE CAUSE AT THIS POINT, TROUBLE SHOOTING IS CURRENTLY IN PROGRESS, SUSPECTING EITHER PROP GOV OR OVERSPEED GOV.

Source: SDR JDWA118SF1 · FAA SDRS
B · 2008-02-18 Matched by certificate designator
N118SF · ATA 2400

ON MONDAY THE 18TH OF FEBRUARY 2008, BEECH 99, N118SF, S/N U-32, SUBURBAN AIR FREIGHT POSITIONING FLIGHT, ROUTE NUMBER SUBAIR 13 OPERATING UNDER PART 91, DEPARTED OMAHA, NE EN ROUTE TO MOLINE, IL. AT APPROXIMATELY 20:30 HOURS JUST NORTH OF MUSCATINE, IA CENTER CLEARED THE FLIGHT FOR DESCENT OUT OF 9000 FT. PASSING THRU 8000 FT, THE PILOT SMELLED SMOKE AND AT THAT TIME THE PILOT NOTICED A GLOW COMING FROM INSIDE OF THE CENTER CONTROL COLUMN AND NOTICED A REFLECTION ON THE TOE OF HIS RIGHT SHOE. THE PILOT SHUT DOWN THE ELECTRICAL SYSTEMS AND PROCEEDED TO GET THE FIRE EXTINGUISHER OUT. FIRE EXTINGUISHER WAS NOT USED, AS THE GLOW AND THE SMOKE STOPPED. DECLARED AN EMERGENCY AND CONTINUED TO MOLINE, LANDED WITHOUT FURTHER PROBLEMS.

Source: SDR JDWA2008SAF01 · FAA SDRS
O · 2005-10-05 Matched by certificate designator
N650DA · ATA 3230

RT MAIN GEAR OLEO STRUT WOULD NOT COMPRESS AFTER LANDING, MORE THAN 50 PERCENT OF NORMAL. AC WAS JACKED, SERVICE OF THE STRUT WAS CHECKED NORMALLY. NEX LANDING, STRUT WOULD AGAIN NOT COMPRESS. OLEO WAS REMOVED FROM AC AND DISASSEMBLED. METERING PIN INSIDE STRUT WAS LOOSE AND MOVING AROUND INSIDE THE STRUT. FUTURE EXAMINATION OF METERING PIN REVEALED THAT NYLON THREAD LOCKING DEVICE SHOWED NO EVIDENCE OF EVER CONCTIGN THE THREADS INSIDE THE UPPER BARREL. THE LOCKING DEVVICE WAS TOO DEEP IN CRCESS PROVIDED IN METERING PIN. THIS CONDITION DID NOT PROVIDE SELF-LOCKING FEATURE THUS ALLOWED PIN TO ROTATE AND COME LOOSE. DAMAGE TO UPPER BARREL OF OLEO WAS EXTENSIVE AND HAD TO BE REPLACED.

Source: SDR JDW2005F00000 · FAA SDRS
J · 1998-04-06 Matched by certificate designator
N118SF · ATA 3231

PIC REPORTED THE INABILITY TO EXTEND THE LANDING GEAR ELECTRICALLY, WITH A LOUD BANG NOTED IMMEDIATELY UPON EXTENSION. THE LANDING GEAR WAS EXTENDED MANUALLY, AND THE AIRCRAFT LANDED WITHOUT FURTHER INCIDENT. SUBSEQUENT INVESTIGATION DISCLOSED A TRIPPED LANDING GEAR CIRCUIT BREAKER, AND A BENT RT OUTBOARD MLG DOOR ACTUATING CAM. THE GEAR DOOR ROLLER ASSY STRUCK THE UNDERSIDE OF THE LANDING GEAR ACTUATING CAM CAUSING THE GEAR TO BIND IN THE WHEEL WELL. INVESTIGATION FAILED TO DETERMINE A CAUSE. THE CAM ASSY MAY HAVE BEEN MIS-RIGGED, OR FAILED TO SNAP OVERCENTER DUE TO WEAK RETURN SPRINGS.

Source: SDR 98ZZZX1689 · FAA SDRS
E R K · 1997-11-13 Matched by certificate designator
N31P · ATA 8520

AIRCRAFT WAS AT CRUISE POWER SETTING. THE PILOT EXPERIENCED A ROUGH RUNNING ENGINE. HE SECURED THE ENGINE AND CONTINUED TO LAND WITHOUT FURTHER INCIDENT. UPON INSPECTION OF THE ENGINE, DETERMINED THE CONNECTING ROD BOLT FAILED ON THE NR 5 CYLINDER AND THE CYLINDER WAS FORCED OFF ITS PAD CAUSING EXTERNAL DAMAGE TO THE ENGINE.

Source: SDR 97ZZZX5143 · FAA SDRS
J · 1995-11-29 Matched by certificate designator
N719GL · ATA 3230

TUS - CREW ELECTED AN AIR TURN BACK AFTER DETERMINING THAT THE NOSE GEAR WOULD NOT RETRACT. MAINTENANCE TROUBLE SHOT AND SERVICED THE GEAR SYSTEM. PERFORMED RETRACTION TESTS WHICH SHOWED NO BINDING, HESITATION, OR OTHER FAULTS. NO FAULT FOUND.

Source: SDR 96ZZZM79 · FAA SDRS
J · 1995-04-18 Matched by certificate designator
N719GL · ATA 6120

ON TAKEOFF, JUST AFTER ROTATION, NR 1 ENGINE LOST POWER. RPM DROPPED, TORQUE WENT TO 4500 LBS PROP WOULD NOT FEATHER WITH PROP LEVER. PROP WAS FEATHERED BY SHUTTING DOWN ENGINE. MAINTENANCE INSPECTED ALL CONTROLS AND LINKAGE. FOUND BETA CABLE STOP BALL UNSEATED AT FORWARD END. RIGGED THROTTLE CABLE TO BETA VALVE. PERFORMED GROUND RUNS AND MAINTENANCE IAW PWA MM 76-16-01. FLEET CAMPAIGN CONDUCTED. NO OTHER PROBLEMS FOUND. (W)

Source: SDR 95ZZZW696 · FAA SDRS
J · 1995-04-18 Matched by certificate designator
N719GL · ATA 6120

ON TAKEOFF, JUST AFTER ROTATION, NR 1 ENGINE LOST POWER. RPM DROPPED, TORQUE WENT TO 4500 LBS PROP WOULD NOT FEATHER WITH PROP LEVER. PROP WAS FEATHERED BY SHUTTING DOWN ENGINE. MAINTENANCE INSPECTED ALL CONTROLS AND LINKAGE. FOUND BETA CABLE STOP BALL UNSEATED AT FORWARD END. RIGGED THROTTLE CABLE TO BETA VALVE. PERFORMED GROUND RUNS AND MAINTENANCE IAW PWA MM 76-16-01. FLEET CAMPAIGN CONDUCTED. NO OTHER PROBLEMS FOUND. (W)

Source: SDR 95ZZZW697 · FAA SDRS
J · 1995-02-04 Matched by certificate designator
N124GP · ATA 5640

FLT NR 2375 - DEPARTING DEN WAS UNABLE TO PRESSURIZE. AIRCRAFT RETURNED TO DEN WHERE GP EXPRESS MAINTENANCE DEFERRED THE PRESSURIZATION SYSTEM. LATER THAT DAY GP EXPRESS MAINTENANCE FOUND THE INSPECTION WINDOW FOR THE AFT CARGO DOOR LOCK MECHANISM BROKEN. WINDOW WAS REPLACED AND SYSTEM CHECKED SATISFACTORY. AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 95ZZZW465 · FAA SDRS

Linked aircraft

N-numberMake / modelYearStatusLink basis
N103SFBEECH 1900C1990Valid RegistrationMatched by certificate designator
N124GPBEECH 1900C1984Valid RegistrationMatched by certificate designator
N130SFBEECH 1900C1990Valid RegistrationMatched by certificate designator
N131SFBEECH 1900C1990Valid RegistrationMatched by certificate designator
N149SFBEECH 1900C1991Valid RegistrationMatched by certificate designator
N159SFBEECH 1900C1991Valid RegistrationMatched by certificate designator
N208QCMatched by certificate designator
N253SFBEECH 1900C1989Valid RegistrationMatched by certificate designator
N367SFBEECH 1900C1989Valid RegistrationMatched by certificate designator
N719GLBEECH 1900C1984Valid RegistrationMatched by certificate designator