WRIGHT AIR SERVICE INC

Part 135 operator · designator HYTA

Data confidence: Records are linked by certificate number, aircraft registration, or a name match that a reviewer has confirmed. Each record below shows how it was linked.

Also recorded as: WRIGHT AIR SERVICE INC, Wright Air Service, Inc.

Accident & enforcement record

Events that happened, regardless of the operator's own reporting. Each links to its public source.

NTSB accidents & incidents

Acc · 2026-06-22 Operator named in NTSB report
TEXTRON AVIATION INC 208B (N94AW) Minor injury Part 135

Operated by Wright Air Service, Inc (per NTSB report)

Not yet finalized — may be revised.
Source: NTSB case ANC26LA062
Acc · 2025-09-22 Operator named in NTSB report
CESSNA 208B (N976E) None injury Part 135

Operated by WRIGHT AIR SERVICE INC (per NTSB report)

Source: NTSB case ANC25LA110
Acc · 2024-06-08 Operator named in NTSB report
CESSNA 206 (N8795Q) None injury Part 135

Operated by Wright Air Service Inc (per NTSB report)

Source: NTSB case ANC24LA046
Acc · 2023-09-16 Operator named in NTSB report
HELIO H-295 (N713C) None injury Part 135

Operated by WRIGHT AIR SERVICE INC (per NTSB report)

Source: NTSB case ANC23LA082
Acc · 2021-08-16 Operator named in NTSB report
CESSNA 208 (N97HA) None injury Part 135

Operated by WRIGHT AIR SERVICE INC (per NTSB report)

Source: NTSB case ANC21LA073
Acc · 2020-09-10 Operator named in NTSB report
Helio H 295 (N68857) None injury Part 135

Operated by Wright Air Service, Inc. (per NTSB report)

Source: NTSB case ANC20CA092
Acc · 2016-09-25 Operator named in NTSB report
HELIO H-295 (N68857) None injury Part 135

Operated by Wright Air Service (per NTSB report)

Source: NTSB case ANC16LA071
Acc · 2016-09-16 Operator named in NTSB report
HELIO H 295 (N6464V) None injury Part 135

Operated by Wright Air Service (per NTSB report)

Source: NTSB case ANC16LA067
Acc · 2016-01-02 Operator named in NTSB report
CESSNA 208B (N540ME) Serious injury Part 135

Operated by WRIGHT AIR SERVICE INC (per NTSB report)

Source: NTSB case ANC16LA012
Acc · 2015-09-13 Operator named in NTSB report
HELIO H 295 (N6464V) None injury Part 135

Operated by Wright Air Service (per NTSB report)

Source: NTSB case ANC15LA070
Acc · 2014-11-14 Operator named in NTSB report
HELIO H 295 (N6465V) None injury Part 135

Operated by Wright Air Service (per NTSB report)

Source: NTSB case ANC15LA004
Acc · 2012-01-26 Operator named in NTSB report
HELIO H-295 (N713C) None injury Part 91

Operated by Wright Air Service (per NTSB report)

Source: NTSB case ANC12CA020
Acc · 2011-12-15 Operator named in NTSB report
PIPER PA-31-350 (N9FW) None injury Part 135

Operated by WRIGHT AIR SERVICE INC (per NTSB report)

Source: NTSB case ANC12CA015
Acc · 2009-03-13 Operator named in NTSB report
HELIO H-295 (N6478V) None injury Part 135

Operated by WRIGHT AIR SERVICE INC (per NTSB report)

Source: NTSB case ANC09LA023
Acc · 2008-09-01 Operator named in NTSB report
CESSNA 207 (N91027) Minor injury Part 135

Operated by Wright Air Service, Inc. (per NTSB report)

Source: NTSB case ANC08CA114
Accident · 1992-07-14 Matched by aircraft (N-number)
Helio H-295 (N68857) None injury
Source: NTSB case SEA92LA155

FAA enforcement actions

FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.

Maintenance disclosure history

Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.

47 reports on file.

O · 2018-12-07 Matched by certificate designator
N8264 · ATA 5753

WHEN CONDUCTING A ROUTINE APPROVED MODIFICATION OF THE RIGHT FLAP WE FOUND THAT THERE WAS A CRACK IN THE AFT INBOARD SPAR (P/N 2625005-18 AT THE BEND RADIUS BETWEEN WS68 AND WS53.5. THE AIRCRAFT HAS A TOTAL TIME OF 3700 HOURS ON IT WHEN THE CRACK WAS DISCOVERED. WE SUBMITTED A SIMILAR M/D REPORT WITH AN INCIDENT DATE OF 04/26/18 AND THE OPINIONS PUT FORTH IN THAT ON HOLD TRUE. THE SKIN AD RIBS IN THIS AREA SHOULD BE MADE OF A THICKER ALUMINUM AND THE RIBS MAY NEED TO MIRROR THE FRONT SPAR IN NUMBER.

Source: SDR 2018F00160 · FAA SDRS
O · 2018-09-27 Matched by certificate designator
N750RV · ATA 3243

NO BRAKES WERE NOTED BY PILOT FOR LEFT TIRE. MAINTENANCE INSPECTED AIRCRAFT AND DETERMINED THAT THE LEFT BRAKE MASTER CYLINDER HAD FAILED. THE UNIT IS SUSPECTED TO HAVE INTERNAL LEAKAGE. UNIT WAS REPLACED AND NO FURTHER ISSUES WERE NOTED

Source: SDR EPUA20180928001 · FAA SDRS
O · 2017-08-07 Matched by certificate designator
N750RV · ATA 3240

DURING AIRCRAFT GROUND OPERATIONS, IT WAS NOTED THAT THE LEFT WHEEL BRAKE CALIPER WAS DISCOVERED BROKEN. MAINTENANCE INSPECTED THE DEFECT AND NOTED THAT THE LEFT MAIN LANDING GEAR BRAKE CALIPER ANCHOR BOLT BROKEN. REPLACED THE BRAKE ASSEMBLY, TORQUE PLATE, AND WHEEL ASSEMBLY. THE BRAKE ASSEMBLY HAD ACCUMULATED 422.5 HRS. SINCE DETAILED BENCH INSPECTION.

Source: SDR EPUA20170807001 · FAA SDRS
O · 2017-07-18 Matched by certificate designator
N750RV · ATA 5520

THE RIGHT ELEVATOR HAS SMOKING RIVETS ON THE INBOARD BUTT RIB WHERE THE TORQUE TUBE ATTACHES. VISUAL INSPECTION INDICATES THAT ALL OF THE ATTACH RIVETS EXCEPT FOR THREE ARE SMOKING. THE LEFT ELEVATOR LOOKS CONSIDERABLY BETTER THAN THE RIGHT SIDE BUT ONE RIVET HAS A BIT OF SMOKE COMING OFF OF IT.

Source: SDR EPUA20170718001 · FAA SDRS
B R J · 2016-06-06 Matched by certificate designator
N713C · ATA 8550

A DISCREPANCY WAS NOTED BY PILOT OF HIGH OIL PRESSURE, A MECHANIC WAS SOON DISPATCHED TO TURN THE OIL PRESSURE DOWN. HE TURNED DOWN THE OIL PRESSURE FROM THE OIL RELIEF VALVE AND REINSTALLED IAW ENGINE MFG DATA, WHEN COMPLETE HE PERFORMED AN OPS AND LEAK CHECK WHICH WAS SATISFACTORY. A WEEK LATER THE OIL RELIEF VALVE CAME LOOSE IN FLIGHT, THE PILOT HAD A PUFF OF SMOKE INTO THE COCKPIT AND TURNED OFF THE MASTER SWITCH, THE SMOKE MOMENTARILY WENT AWAY BUT THEN THE ENGINE STARTED TO RUN ROUGH WITH PARTIAL RPM LOSS. THE PILOT TURNED BACK TO AIRPORT AND LANDED. HE INSPECTED THE ENGINE FINDING SUBSTANTIAL OIL ON COWLING AND CALLED FOR MAINTENANCE SUPPORT. WHEN MAINTENANCE SUPPORT ARRIVED, HE FOUND THE REGULATOR HAD BACKED OFF ENOUGH TO OVERBOARD DUMP ALL THE ENGINE OIL. WHEN INSPECTED, HE FOUND THE OIL RELIEF VALVE WAS ADJUSTED ALMOST ALL THE WAY OUT WITH SEVERAL THREADS LEFT ON THE RELIEF VALVE SCREW TO GET THE ENGINE INTO THE GREEN PRESSURE RANGE. WE BELIEVE THE SMALL AMOUNT OF THREADS WITH LONG SAFETIES IN PLACE ALLOWED THE REGULATOR TO BACK OUT. WE'RE DEVELOPING A NEW PROCEDURE AND RII TO VERIFY THREAD LENGTH BEFORE RELEASING AIRCRAFT BACK TO SERVICE.

Source: SDR HYTA201606060001 · FAA SDRS
J · 2016-04-22 Matched by certificate designator
N750RV · ATA 7260

STANDBY POWER ANNUNCIATOR LIGHT WON’T GO OUT. INSPECTED ACFT & FOUND THAT THE RETAINING RING FOR THE STANDBY ALTERNATOR DRIVE PULLEY HAD FAILED. DUE TO THIS FAILURE THE DRIVE PULLEY HAD MIGRATED OUT OF THE HOUSING ASSEMBLY & WAS LYING IN THE ENG COWLING ASSEMBLY. THE DRIVE ASSEMBLY WAS REPLACED AS AN ASSEMBLY.

Source: SDR EPUA20160422001 · FAA SDRS
O · 2015-08-29 Matched by certificate designator
N6478 · ATA 5714

CRACKS FOUND IN UPPER TUBE OF CARRY THRU ASSEMBLY, PN 391-030-401-30, AT LOW POINT OF THE TWO CUT OUTS WHICH ARE MILLED IN THE TUBE TO ALLOW INSTALLATION OF WING ATTACH BOLT. THE MILLING PROCESS LEFT A SHARP EDGE THAT CREATED A STRESS RISER. THIS IS A CRITICAL FACTOR CONTRIBUTING IN HOW THESE CRACKS DEVELOP. WE HAVE SINCE DRESSED THE SHARP EDGES ON OUR OTHER CARRY THRU ASSEMBLIES TO FORM A 1/8" RADIUS POLISHED BULL NOSE PROFILE.

Source: SDR HYTA20150908001 · FAA SDRS
O · 2015-08-27 Matched by certificate designator
N713C · ATA 5714

CRACKS FOUND IN CARRY THRU ASSEMBLY AT LOW POINT OF MILLED CUT OUTS IN UPPER TUBE OF ASSEMBLY. THE MILLING PROCESS LEFT A SHARP EDGE CREATING A STRESS RISER. THIS WAS A FACTOR CONTRIBUTING TO CRACKS DEVELOPING. WE HAVE DRESSED OUR OTHER CARRY THRU ASSEMBLIES TO A 1/8" RADIUS POLISHED BULL NOSE PROFILE.

Source: SDR HYTA20150904001 · FAA SDRS
R · 2015-06-30 Matched by certificate designator
N59764 · ATA 8530

AFTER COMPLETING ROUTINE LANDING, PILOT NOTED THAT THE LT ENGINE WAS RUNNONG ROUGH ON GROUND WITH HIGH MANIFOLD PRESSURE AND THE LT FUEL FLOW INDICATED ZERO IN FLIGHT WHEN LEANED. ON INVESTIGATION, THE LEFT ENGINE CYLINDER NR 4 EXHAUST VALVE SEAT WAS DISLODGED AND WAS PREVENTING THE EXHAUST VALVE FROM CLOSING. THE PISTON WAS GOUGED BY THE PARTIALLY OPEN EXHAUST VALVE AND A PORTION OF CYLINDER MATERIAL WAS MISSING BETWEEN THE SPARK PLUG HOLE AND THE DISLODGED VALVE SEAT. THIS ENGINE HAS BEEN INSTALLED SINCE APRIL 21, 2015 AND HAD ACCRUED 166.4 HOURS SINCE OVERHAUL.

Source: SDR 2015F00076 · FAA SDRS
O · 2014-03-07 Matched by certificate designator
N32WA · ATA 2210

SERVO, FAILURE OF THE TACH GENERATOR.

Source: SDR HYTA2014F00084 · FAA SDRS
O · 2013-04-30 Matched by certificate designator
N713C · ATA 5524

CRACKS FOUND IN .025 ALUMINUM WEB RIVETED TO FORWARD SIDE OF STABILATOR HORN ASSEMBLY P/N 250-020-401.

Source: SDR HYTA2013043000010 · FAA SDRS
O · 2013-04-30 Matched by certificate designator
N713C · ATA 5514

WHILE PERFORMING A 100 HOUR INSPECTION A .5 INCH CRACK WAS FOUND RADIATING FROM THE LIGHTENING HOLE IN .063" STEEL COVER/SPLICE PLATE, P/N 391-020-305-2 BOLTED TO FORWARD SIDE OF HORIZONTAL STABILATOR CENTER BOX/SPLICE STRUCTURE. THIS STRUCTURE ATTACHES THE LEFT AND RIGHT HORIZONTAL TAIL ASSEMBIES (P/N'S 250-020-001-0 AND -1) TOGETHER.

Source: SDR HYTA2013043000012 · FAA SDRS
O · 2013-04-22 Matched by certificate designator
N713C · ATA 5510

DURING A ROUTING 100HR/ANNUAL INSPECTION, CRACKS WERE FOUND IN SUPPORTING .025 WEB OF HORIZONTAL STABILATOR HORN ASSY AND ALSO A CRACK RADIATING FROM LIGHTNING HOLE OF .063 FORWARD COVER PLATE (PN 391-020-305-2) THAT IS PART OF THE BOLTED ASSEMBLIES SECURING THE 2 STABILATOR HALFS TOGETHER.

Source: SDR HYTA2013F00090 · FAA SDRS
O · 2013-01-14 Matched by certificate designator
N999WV · ATA 2562

UNIT FAILED 97.207, D-CHECK THIS IS 1 OF 7 UNITS THAT HAVE FAILED IN THE LAST YEAR.

Source: SDR HYT2013F00000 · FAA SDRS
L · 2011-12-27 Matched by certificate designator
N900WA · ATA 2562

ELT FAILED G-SWITCH TEST.

Source: SDR 2011FA0000807 · FAA SDRS
L · 2011-12-27 Matched by certificate designator
N32WA · ATA 2562

ELT FAILED G-SWITCH TEST.

Source: SDR 2011FA0000808 · FAA SDRS
L · 2011-12-27 Matched by certificate designator
N4365U · ATA 2562

ELT FAILED G-SWITCH TEST.

Source: SDR 2011FA0000809 · FAA SDRS
O · 2011-08-09 Matched by certificate designator
N976E · ATA 2562

ANTENNA, PN 110-773 APPEARS TO BE BROKEN INTERNALLY. THE TOP PORTION OF THE ANTENNA, INCLUDING THE WIRE WHIP, CAN BE EASILY LIFTED OFF THE BASE. VISUAL INSP ALONE WILL NOT REVEAL THIS DISCONNECT. THIS ANTENNA IS PART OF THE ME406 ELT SYSTEM. THIS IS THE 4TH INCIDENT OF THIS CONDITION ON VARIOUS AIRPLANES IN THE FLEET ALL OF WHICH HAD LOWER TIME AND CYCLES ON THE ANTENNA THAN THIS ONE.

Source: SDR 2011FA0000511 · FAA SDRS
L · 2011-04-15 Matched by certificate designator
N1314X · ATA 2562

ELT G-SWITCH FAILED TEST.

Source: SDR 2011FA0000806 · FAA SDRS
O · 2010-10-25 Matched by certificate designator
N4637U · ATA 8011

HAVE HAD A CHRONIC PROBLEM WITH BREAKAGE OF STARTER CLUTCH SPRING PN 643109 WHICH IS A COMPONENT OF STARTER ADAPTER PN 643259A. THERE HAVE BEEN 9 FAILURES OF THIS SPRING IN 1592 HRS OF OPERATION. AVERAGE TIS HAS BEEN 173 HRS, WORST TIS 18 HRS, BEST TIS 422 HOURS. PROBLEM PERSISTS EVEN AFTER REPLACING ENGINE WITH NEW ENGINE WITH FAILURES AT 90 TIS AND 701 STIS. MAG TIMING HAS ALWAYS BEEN FOUND AT SEC MAGS, STARTER CONTACTOR, AND MAG SWITCH HAVE ALL BEEN REPLACED IN PURSUING CAUSE OF THESE FAILURES. THE CROSS SECTION OF THE CLUTCH SPRING FOR THIS CURRENT ADAPTER IS SMALLER THAT THE SPRING FOR THE EARLIER STYLE STARTER ADAPTER.

Source: SDR HYT2010F00001 · FAA SDRS
O · 2010-02-15 Matched by certificate designator
N1314X · ATA 2720

AFTER A "HEADS UP" FROM ANOTHER OPERATOR, THE RUDDER TORQUE TUBE PN 2633066-3 WAS INSPECTED FOR CORROSION. INITIAL INSP REAVEALED CORROSION ON MUCH OF THE EXPOSED SURFACES OF THE FRAME, PN 2633014-1 AND SUPPORT PLATE PN 2633017-1 WHICH ARE LOCATED INSIDE THE RUDDER. THE LOWER PORTION OF THE TUBE AND BELLCRANK EXTENDING OUTSIDE THE RUDDER WAS COATED WITH FINISH PAINT AND WAS NOT AFFECTED. THE TORQUE TUBE ASSY WAS REMOVED FROM THE RUDDER AND CORROSION WAS FOUND ON ALL THE EXPOSED SURFACES AS WELL AS THE FAY SURFACES. THERE WAS MILD CORROSION INSIDE THE TUBE NEAR EACH END. THE PRIMER APPLIED TO THESE SURFACES APPEARS TO BE THIN AND NOT THE SAME QUALITY AS PRIMER ON ADJACENT ALUMINUM SKINS AND RIBS. ALL ORIGINAL PAINT WAS REMOVED FROM TORQUE TUBE ASSY AND MINIMAL DAMAGE WAS NOTED. PART WAS RECOATED WITH EPOXY PRIMER AND REINSTALLED USING PROCEDURES OUTLINED IN CAB06-2. CAB06-2 COVERS THIS SAME SUBJECT BUT DOES NOT INCLUDE THIS S/N ACFT. THIS ACFT IS EQUIPPED WITH TKS ANTI-ICE SYS AND TKS FLUID WAS FOUND THROUGH THIS AREA INCLUDING INSIDE THE RUDDER AND BETWEEN FAY SURFACES. ALSO ALL 4 FLAP AFT BELLCRANKS AND LT FWD BELLCRANK WERE IN SIMILAR CONDITION AND HAD TO BE STRIPPED AND REPAINTED.

Source: SDR HYT2010F00000 · FAA SDRS
O · 2010-01-07 Matched by certificate designator
N1314X · ATA 5343

RT MLG TRUNNION WAS FOUND CHAFED AND WORN BEYOND LIMIT BY CONTACT WITH MLG FAIRING PN 2641018-28. WEAR LIMIT IS ESTABLISHED IN CAB05-17 WHICH ADDRESSES THIS CONDITION IN EARLIER SN AIRPLANES BUT DOES NOT COVER THIS AIRPLANE MFG 6/5/08. CONDITION WAS NOT DETECTED UNTIL MLG WAS REMOVED FOR SCHEDULED CORROSION INSP ALTHOUGH THE AREA IS EASILY INSPECTED WITH THE FAIRING REMOVED. AIRPLANE CAME FROM FACTORY WITH NO RUB STRIP ON THE TRUNNION OR RUBBER MOLDING ON THE LOWER EDGE OF THE FAIRING AS CALLED FOR IN CAB05-17. THIS AREA SHOULD BE INSPECTED ANY TIME THE FAIRING IS REMOVED ON EITHER SIDE.

Source: SDR 2010FA0000099 · FAA SDRS
K · 2008-02-26 Matched by certificate designator
N91027 · ATA 2820

METERED FUEL PRESSURE HOSE FAILED. THIS HOSE RUNS FROM THE FUEL INJECTOR DISTRIBUTOR TO THE FIREWALL. LOW PRESSURE TEST OF FAILED HOSE REVEALED MULTIPLE LEAKS ALONG LENGTH OF HOSE. HOSE WAS INSTALLED NEW ON 4/8/03/ HOSE FAILURE NOTED ON 2/26/08 WHEN ENGINE WOULD NOT CONTINUE TO RUN. FOLLOWING INFO ON HOSE TAG: STRATOFLEX PT/BA, 156MA001-3SO350, CD1Q02WO8316, OP1500PSI, TSOC53A, C751/II-A-S/P, A12/12/02, OT275F. HOSE WAS PART OF HOSE KIT 2738916 DATED 12/12/02. IN RECENT PAST SAME HOSE ON ANOTHER AIRCRAFT IN FLEET HAD SAME TYPE OF FAILURE AT APPROX 1600 HRS IN SERVICE. (K)

Source: SDR HYT2008F00000 · FAA SDRS
O · 2007-06-06 Matched by certificate designator
N4365U · ATA 2720

ON A ROUTINE INSPECTION, A MECHANIC FOUND THAT THE PILOTS RT RUDDER PEDAL PIN WAS ABOUT TO FALL OUT OF THE RUDDER PEDAL. FURTHER INSPECTION FOUND THAT THE ROLL PIN PN: NAS561C318 HAD FALLEN OUR OF ITS HOLE CAUSING THE RUDDER PEDAL PIN TO MIGRATE FROM ITS POSITION. INSPECTION OF RUDDER PEDAL ASSY FOUND THAT THE ROLL PIN HOLE IN THE RUDDER PEDAL HAD BECOME ENLARGED, DUE TO AN UNKNOWN REASON. RECOMMENDATION TO PREVENT RECURRENCE: ATTENTION TO ROLL PIN INSTALLATION FOR ADEQUATE PRESS FIT AND ADDITIONAL ATTENTION OF ROLL PIN ON ROUTINE INSPECTION. (K)

Source: SDR 2007FA0000573 · FAA SDRS
O · 2007-04-17 Matched by certificate designator
N4365U · ATA 7810

CRACKING OCCURRED IN A SHORT TIME SPAN, DURING NORMAL OPERATION. CRACKS WERE OVER AN AREA APPROX 7 INCHES X 7 INCHES. ONE PIECE APPROX 3 INCHES X 3 INCHES SEPARATED FROM THE PART. AFTER CRACKING, DEFORMATION OF LOWER TRAILING EDGE OCCURRED BECAUSE IT WAS NO LONGER RIGID. IF THIS PROBLEM HAD GONE UNNOTICED, HEAT DAMAGE WOULD PROBABLY HAVE OCCURRED TO ADJACENT PARTS. MATERIAL OR MFG PROCESS COULD BE SUSPECT. RECENT MFG BULLETIN CAB 07-2 AFFECTS SOME PRIMARY EXHAUST DUCTS DUE TO IMPROPER MFG, BUT IT DOES NOT APPLY TO THIS ONE. (MFG HAS BEEN MADE AWARE OF THIS PROBLEM, PART WAS RETURNED TO THEM ON REQUEST FOR EVALUATION). (K)

Source: SDR 2007FA0000355 · FAA SDRS
O · 2007-04-01 Matched by certificate designator
N900WA · ATA 5730

SMOKING RIVETS IN LEADING EDGE SKIN UPPER SEAM. EVERY COUNTERSUNK HOLE FROM WS 35 TO WS 141 WAS FRETTING AGAINST THE RIVET HEAD. SAME CONDITION TO SAME EXTENT ON BOTH WINGS. IT APPEARS THE SKIN WAS COUNTERSUNK TOO DEEPLY. SAME CONDITION TO LESSER EXTENT FOUND ON OTHER AC IN THE FLEET. MFG ADDRESSES THIS ISSUE IN THE SRM WITH (2) TYPES OF REPAIR DEPENDING ON SEVERITY OF DAMAGE. (K)

Source: SDR HYT2007F00000 · FAA SDRS
O · 2005-02-18 Matched by certificate designator
N900WA · ATA 3710

INSTRUMENT VACUUM SYSTEM HAD INSUFFICIENT SUCTION. ADJUSTING THE VACUUM REGULATOR HAD NO EFFECT. LOOKING THROUGH THE VACUUM EJECTOR OUTLET REVEALED A FOREIGN OBJECT RESTRICTING THE VENTURI. AN 8-32 NUT WAS RETRIEVED FROM THE VENTURI. THIS NUT CAME FROM INSIDE THE BLEED AIR RELIEF VALVE, PN RV05-268, WHICH IS MOUNTED ADJACENT TO THE INLET SIDE OF THE VENTURI. THIS NUT IS USED AS A JAM NUT TO SECURE THE RELIEF VALVE PRESSURE SETTING. SUGGEST THIS NUT COULD BE SECURED WITH LOCKTITE OR OTHER THREAD LOCKER. (K)

Source: SDR HYTA2005005 · FAA SDRS
O · 2004-12-23 Matched by certificate designator
N32WA · ATA 3213

TUBE OF NOSE GEAR STRUT TUBE ASSY PN 26430161, CAME LOOSE FROM UPPER END CAP ALLOWING TUBE TO FLOAT WITH NOSE GEAR STRUT MOVEMENT. VENT TUBE INSIDE STRUT TUBE WAS CRUSHED AND SHOVED TO UPPER END OF TUBE. EXAMINATION OF TUBE AND END CAP REVEALED THAT END CAP WAS ONLY ABOUT 60 PERCENT BONDED TO TUBE. NEW ASSEMBLY FROM MFG HAS GAPS IN BONDING AGENT AND IS LESS THAN 100 PERCENT BONDED. (AL01200501892)

Source: SDR HYTA2M5004 · FAA SDRS
O · 2004-11-19 Matched by certificate designator
N976E · ATA 7220

FELT SEALING STRIP APPROXIMATELY .5 INCH X 7 INCHES WAS COMING LOOSE FROM INSIDE THE ENGINE INDUCTION AIR PLENUM. OFFENDING FELT STRIP WAS REMOVED AS IT SERVES NO PURPOSE. THIS STRIP WAS LOCATED AT ABOUT 4 O’CLOCK ON THE INSIDE SURFACE ACROSS THE RT END OF THE LOWER PLENUM PANEL PN 2658039-19. LOCATION OF STRIP COINCIDES WITH LOWER END OF ACCESS PANEL PN 2658039-1 WHICH HAS PROPERLY POSITIONED FELT SEALING STRIPS.

Source: SDR HYTA2005003 · FAA SDRS
O · 2004-10-29 Matched by certificate designator
N900WA · ATA 3213

SHOT PEENED LOWER SURFACE OF MAIN GEAR CENTER SPRING IS BEING DAMAGED BY CONTACT WITH RIVETS AND SCREWS PROTRUDING FROM THE MLG COVER WHICH IS LOCATED BENEATH THE CENTER SPRING. THIS IS THE THIRD AIRCRAFT FOUND IN THIS CONDITION.

Source: SDR HYTA2005002 · FAA SDRS
O · 2004-10-20 Matched by certificate designator
N540ME · ATA 3210

FLEXING OF MLG SPRING CAUSES CENTER SPRING TO CONTACT MLG COVER PN 2611103-10 WHICH IS LOCATED BENEATH THE CENTER SPRING. TWO RIVETS HAD WORN INTO THE CENTER SPRING LOWER SURFACE. THESE RIVETS ARE THE CENTER IB RIVETS THAT FASTEN A FAIRING AT EACH END OF THE COVER. SUGGEST ELIMINATING THE CENTER RIVET AND INSTALLING TWO RIVETS FURTHER OB AND OFF CENTER AT BOTH FAIRINGS. THE CENTER SPRING WAS ALSO CONTACTING SCREWS THAT SECURE A COVER THAT ACCESSES THE MLG DEICE PLUMBING. THESE SCREWS COULD BE .1250 INCH SHORTER. NO DAMAGE EXCEEDED .005 INCHES IN DEPTH. ALSO RECOMMEND VINYL CHAFE TAPE ON LOWER SURFACE OF CENTER SPRING.

Source: SDR HYTA2005001 · FAA SDRS
O · 2004-08-02 Matched by certificate designator
N976E · ATA 5711

LOWER SURFACE OF LT AND RT FORWARD WING SPARS AND LIFT STRUT ATTACH FITTINGS HAVE BEEN CHAFED BECAUSE OF CONTACT WITH THE LIFT STRUT UPPER FAIRING/COVER. WORST DAMAGE WAS LESS THEN .005 INCH IN DEPTH AND WAS EASILY BLENDED OUT. APPLIED VINYL CHAFE TAPE TO SPAR AND STRUT FITTINGS TO PREVENT REOCCURRENCE. CAB02-2 REV 1 ADDRESSES THIS CONDITION BUT DOES NOT INCLUDE THIS S/N AIRPLANE. IT APPEARS THAT MFG CHANGED THE RIVET PATTERN IN THIS FAIRING/COVER ASSEMBLY, P/N 2621012-54 AND 55 ON LATER S/N AIRPLANES TO AVOID DAMAGE CAUSED BY RIVET HEADS. BUT FURTHER REDESIGN MAY BE NECESSARY TO ELIMINATE THE PROBLEM. APPLICATION OF CHAFE TAPE EFFECTIVELY PREVENTS DAMAGE. (M)

Source: SDR HYTA2004007 · FAA SDRS
O · 2004-04-23 Matched by certificate designator
N4365U · ATA 5313

LT LONGERON 261310531 AND RT LONGERON 261310528 WERE FOUND CRACKED AT THE LOWER AFTER CORNERS OF THE CUT-OUTS FOR THE CONTROL COLUMN TORQUE TUBE. THESE CUT-OUTS ARE LOCATED JUST FORWARD OF THE NOSE GEAR SPRING SUPPORT FITTINGS 26430633. RT LONGERON HAS ONE CRACK .3750 INCH LONG AND A SECOND CRACK .7500 INCH LONG EXTENDING DOWN AND AFT TO THE NEAREST RIVET. LT LONGERON HAS ONE CRACK .7500 INCH LONG EXTENDING DOWN AND AFT TO THE NEAREST RIVET. PROBABLE CAUSE IS LOADS IMPOSED BY THE NOSE GEAR SPRING SUPPORTS AT A POINT WHERE THE LONGERON WEB HAS BEEN MOSTLY REMOVED TO CLEAR THE CONTROL COLUMN TORQUE TUBE. THIS DAMAGE CAN BE REPAIRED WITH A RIVETED DOUBLER OF HEAVIER MATERIAL.

Source: SDR HYTA2004006 · FAA SDRS
K · 2004-03-25 Matched by certificate designator
N59764 · ATA 7921

ON 24 MAR 04, AC DEPARTED, AT APPROX 50 MILES FROM DEPARTURE, PILOT NOTICED A LOSS OF MANIFOLD PRESSURE AND A LOSS OF OIL PRESSURE ON THE LT ENGINE, FEATHERED THE LT PROPELLER, SHUT DOWN THE LT ENGINE AND RETURNED TO DEPARTURE. A MAINTENANCE INSPECTION REVEALED THAT THE LT OIL COOLER HAD RUPTURED, LEAKING OIL FREELY. MAINT HAS ELECTED TO REPLACE THIS ENGINE.

Source: SDR WVB2004F00000 · FAA SDRS
O · 2004-03-17 Matched by certificate designator
N4365U · ATA 1430

WHILE CONDUCTING INITIAL INSPECTION, BOTH AFT WING TO FUSELAGE ATTACH BOLTS WERE FOUND SLIGHTLY RUSTED. DAMAGE WAS NEGLIGIBLE. THESE BOLTS AS WELL AS FORWARD ATTACH BOLTS AND UPPER AND LOWER STRUT ATTACH BOLTS WERE APPARENTLY INSTALLED DRY. THIS HARDWARE SHOULD ALL BE INSTALLED WITH A RUST INHIBITOR OR GREASE.

Source: SDR HYTA2004003 · FAA SDRS
O · 2004-03-17 Matched by certificate designator
N4365U · ATA 3397

FLASHING BEACON WIRE IN TAILCONE WAS ROUTED OVER THE BALLAST RESISTOR WHERE THERE IS LESS THAN .5 INCH CLEARANCE TO STRUCTURE. WIRE WAS NOT TOUCHING BALLAST RESISTOR OR AIRPLANE STRUCTURE, BUT INSULATION WAS BURNED CLEAR THROUGH TO BARE WIRE. WIRE SHOULD HAVE BEEN ROUTED UNDER AND AWAY FROM RESISTOR.

Source: SDR HYTA2004004 · FAA SDRS
O · 2004-03-17 Matched by certificate designator
N4365U · ATA 3210

FLEXING OF MLG CENTER SPRING PN 2641014-3 CAUSES CENTER SPRING TO CONTACT MLG COVER PN 2611103-10 WHICH IS LOCATED BENEATH THE CENTER SPRING. CHAFING HAD WORN THROUGH THE PAINT ON THE LOWER SURFACE OF CENTER SPRING. TWO RIVETS HAD WORN INTO THE LOWER SURFACE OF THE CENTER SPRING. THESE RIVETS ARE THE CENTER IB RIVETS THAT FASTEN A FAIRING AT EACH END OF THE COVER. SUGGEST ELIMINATING THE CENTER RIVET AND INSTALL TWO RIVETS FURTHER OB AND OFF CENTER. ALSO APPLY CHAFE TAPE TO LOWER SURFACE OF CENTER SPRING.

Source: SDR HYTA2004005 · FAA SDRS
O · 2002-12-16 Matched by certificate designator
N54WA · ATA 5320

PART SITS ON TOP OF NLG TUNNEL AND IS PART OF THE GEAR ACTUATOR ATTACH POINT. IT ALSO HAD A TWIST IN IT, PROBABLY FROM STRESS FROM THE ACTUATOR.

Source: SDR HYTA2002001 · FAA SDRS
O · 1999-06-22 Matched by certificate designator
N46374 · ATA 2720

ROD END BROKE WHERE IT EXITS SPACER ASSY, PN 1260632-3, WHICH IS THE RUDDER TRIM SPROCKET AT THE END OF THE STEERING BUNGEE. SUBMITTER STATED THIS IS THE THIRD ONE KNOWN TO BREAK IN 10 YEARS. NO NOSE WHEEL STEERING, BUT STILL RUDDER STEERING.

Source: SDR 99ZZZX2544 · FAA SDRS
O · 1999-01-19 Matched by certificate designator
N9FW · ATA 3230

ARM FOUND CRACKED DURING 100-HOUR INSPECTION. ARM, P/N 42042-00.

Source: SDR 99ZZZX628 · FAA SDRS
K J · 1997-02-24 Matched by certificate designator
N900WA · ATA 2910

AIRCRAFT LOST HYDRAULIC PRESSURE DURING LANDING GEAR EXTENSION CYCLES. REPLACED CRACKED HYDRAULIC LINE IN HELL HOLE. SERVICED RESERVOIR, BLED SYSTEM, LEAK AND FUNCTIONALLY CHECKED GOOD.

Source: SDR 97ZZZX1114 · FAA SDRS
O · 1997-01-29 Matched by certificate designator
N2043X · ATA 8530

NR 5 CYLINDER HAD CRACK AT UPPER SPARK PLUG BOSS. THIS ENGINE HAS HAD C/W SID 97-2, SID 97-3, AND PROPER MAINTENANCE DURING ITS LIFE. BAFFLING, FUEL SYSTEM SETUP, AND GENERAL MAINTENANCE HAVE BEEN CAREFULLY CONTROLLED ON THIS ENGINE.

Source: SDR 98ZZZX875 · FAA SDRS
O · 1997-01-10 Matched by certificate designator
N27755 · ATA 8011

AIRCRAFT LANDED IN FT YUKON AND SHUT DOWN. UPON TRYING TO START THE RIGHT ENGINE, THE BENDIX ENGAGED, BUT STARTER WOULD NOT SPIN THE PROP. STARTER WAS RECENTLY OVERHAULED.

Source: SDR 97ZZZX438 · FAA SDRS
N · 1996-12-02 Matched by certificate designator
N900WA · ATA 3260

RIGHT LANDING GEAR DOWN LIGHT INTERMITTENT. REPLACED RIGHT MAIN GEAR DOWN AND LOCK MICROSWITCH WITH NEW. ADJUSTED AND SWUNG GEAR. CHECKED GOOD. ALL WORK DONE IAW LEAR 25D MM. (X)

Source: SDR 12196900WA · FAA SDRS
O · 1995-09-08 Matched by certificate designator
N4637U · ATA 2730

DURING ROUTINE INSPECTION, FOUND PILOT YOKE PUSH ROD CONTROL TUBE ASSY WITH LOOSE RIVETS. NOTED .05 INCH PLAY IN CONNECTION. NEW PART RECEIVED FROM CESSNA AND INSPECTION REVEALED ALUMINUM RIVETS USED DURING ASSEMBLY IN PLACE OF CARBON STEEL. CESSNA FACTORY VERIFIED CARBON STEEL RIVETS REQUIRED.

Source: SDR 95ZZZX4554 · FAA SDRS
R · 1995-04-12 Matched by certificate designator
N900WA · ATA 7200

LEFT ENGINE RPM ROLLED BACK TO 40 PERCENT AFTER DEPARTURE. UNEVENTFUL LANDING ACCOMPLISHED. FOD DAMAGE NOTED. ENGINE REPLACED WITH SERVICEABLE UNIT. SUBMITTER RECOMMENDATION: AVOID FOD. SUSPECTED ICE INGESTION, NO FOREIGN MATERIAL WAS FOUND ON TEAR-DOWN. OPER CONTROL NR 4-12-95900WA.

Source: SDR 95ZZZX2104 · FAA SDRS
O · 1995-01-07 Matched by certificate designator
N59764 · ATA 8530

OIL BLOWING OUT BREATHER. FOUND NR 1 CYLINDER AT 10/80. PULLED CYLINDER AND FOUND COMP. RINGS BROKEN IN MANY PIECES ABOUT .25 INCH TO 2.5 INCH. THESE RINGS ARE OF WRONG COMPOSITION. (BRITTLE).

Source: SDR 95ZZZX411 · FAA SDRS

Linked aircraft

N-numberMake / modelYearStatusLink basis
N1314XCESSNA 208B2008Valid RegistrationMatched by certificate designator
N1323RCESSNA 208B1999Valid RegistrationMatched by certificate designator
N143WACESSNA 208B2012Valid RegistrationMatched by certificate designator
N2043XBEECH A361978Valid RegistrationMatched by certificate designator
N27755PIPER PA-31-3501978Valid RegistrationMatched by certificate designator
N288PCCESSNA 208B2007Valid RegistrationMatched by certificate designator
N32WACESSNA 208B1991Valid RegistrationMatched by certificate designator
N4365UCESSNA 208B1991Valid RegistrationMatched by certificate designator
N452TTEXTRON AVIATION INC 208B2016Valid RegistrationMatched by certificate designator
N4637UCESSNA U206G1979Valid RegistrationMatched by certificate designator
N540MEOperator named in NTSB report
N54WAPIPER PA-31-3501976Valid RegistrationMatched by certificate designator
N59764PIPER PA-31-3501975Valid RegistrationMatched by certificate designator
N6464VHELIO H-2951969Valid RegistrationMatched by certificate designator
N6464VHELIO H-2951969Valid RegistrationOperator named in NTSB report
N6465VHELIO H-2951969Valid RegistrationOperator named in NTSB report
N6478VHELIO H-2951970Valid RegistrationMatched by certificate designator
N6478VHELIO H-2951970Valid RegistrationOperator named in NTSB report
N68857HELIO H-2951974Valid RegistrationOperator named in NTSB report
N68857HELIO H-2951974Valid RegistrationMatched by certificate designator
N713CHELIO H-2951970Valid RegistrationMatched by certificate designator
N713CHELIO H-2951970Valid RegistrationOperator named in NTSB report
N750RVCESSNA 208B2015Valid RegistrationMatched by certificate designator
N761RVTEXTRON AVIATION INC 208B2016Valid RegistrationMatched by certificate designator
N762RVTEXTRON AVIATION INC 208B2016Valid RegistrationMatched by certificate designator
N8264TEXTRON AVIATION INC 208B2016Valid RegistrationMatched by certificate designator
N8795QCESSNA U206G1976Valid RegistrationMatched by certificate designator
N8795QCESSNA U206G1976Valid RegistrationOperator named in NTSB report
N900WACESSNA 208B1998Valid RegistrationMatched by certificate designator
N91027Operator named in NTSB report
N94AWTEXTRON AVIATION INC 208B2019Valid RegistrationMatched by certificate designator
N94AWTEXTRON AVIATION INC 208B2019Valid RegistrationOperator named in NTSB report
N976ECESSNA 208B2002Valid RegistrationMatched by certificate designator
N976ECESSNA 208B2002Valid RegistrationOperator named in NTSB report
N97HACESSNA 208B1997Valid RegistrationMatched by certificate designator
N97HACESSNA 208B1997Valid RegistrationOperator named in NTSB report
N999WVCESSNA 208B2009Valid RegistrationMatched by certificate designator
N9FWPIPER PA-31-3501974Valid RegistrationOperator named in NTSB report
N9FWPIPER PA-31-3501974Valid RegistrationMatched by certificate designator