CENTRAL AIR SOUTHWEST, INC.
Also recorded as: CENTRAL AIR SOUTHWEST, INC., CENTRAL AIRLINES INC, Central Air Southwest, Central Air Southwest, Inc.
Accident & enforcement record
Events that happened, regardless of the operator's own reporting. Each links to its public source.
NTSB accidents & incidents
Operated by Central Air Southwest (per NTSB report)
Operated by CENTRAL AIR SOUTHWEST INC (per NTSB report)
Operated by Central Air Southwest Inc. (per NTSB report)
Operated by Central Air Southwest (per NTSB report)
Operated by Central Air Southwest (per NTSB report)
FAA enforcement actions
FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.
Maintenance disclosure history
Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.
110 reports on file — showing most recent 50.
LEFT ENGINE FEATHERED DUE TO LOW OIL PRESSURE. NUMBER 2 CYLINDER STUDS BROKEN.
LEFT MAIN LANDING GEAR WOULD NOT FULLY RETRACT AND EXTENDED SLOWLY. THE CLEVIS HAD BROKEN CAUSING ONLY THE AUXILIARY ACTUATOR TO BE FUNCTIONING.
LEFT ENGINE POWER LOSS. RETURNED TO RICHMOND AIRPORT (KRIC).
PILOT HAD LOSS OF OIL PRESSURE ON LT ENGINE AND SHUT ENGINE DOWN AND LANDED AS SOON AS PRACTICAL. A CRACK WAS FOUND ON THE CRANKCASE AT THE TOP FWD STUD HOLE OF THE NR 2 CYLINDER BASE STUD LEADING TO AN OIL GALLEY. NEARLY ALL THE OIL HAD LEAKED OUT.
AFTER LOWERING THE LANDING GEAR THERE WAS NO NOSE GEAR GREEN DOWN AND LOCKED LOCATION. THE PILOT DID A FLY-BY AND THE TOWER THOUGHT ALL 3 GEAR LOOKED DOWN. AFTER LANDING AND CLEARING THE RUNWAY THE NOSE GEAR RETRACTED CAUSING THE NOSE TO SKID ON THE GROUND. IN DOING SO THE NOSE GEAR DOORS INTERFERED WITH THE GROUND CAUSING THEM TO ENTANGLE IN THE NOSE GEAR AND WHEEL WELL. ONCE THE REAR NOSE GEAR DOORS WERE UNENTANGLED THE NOSE GEAR CAME DOWN AND LOCKED AND THE NOSE GEAR LIGHT WAS ON. SINCE THE PILOT DID NOT HAVE AN INDICATION AND THE TOWER THOUGHT IT LOOKED DOWN IT MUST HAVE BEEN NEARLY DOWN BUT NOT LOCKED. THE DRAG BRACE MECHANISM WAS REMOVED AND WE NOTED THE DRAG BRACE SHAFT SHOWED SIGNS OF WEAR.
AFTER LOWERING THE LANDING GEAR THERE WAS NO NOSE GEAR GREEN DOWN AND LOCKED LOCATION. THE PILOT DID A FLY-BY AND THE TOWER THOUGHT ALL 3 GEAR LOOKED DOWN. AFTER LANDING AND CLEARING THE RUNWAY THE NOSE GEAR RETRACTED CAUSING THE NOSE TO SKID ON THE GROUND. IN DOING SO THE NOSE GEAR DOORS INTERFERED WITH THE GROUND CAUSING THEM TO ENTANGLE IN THE NOSE GEAR AND WHEEL WELL. ONCE THE REAR NOSE GEAR DOORS WERE UNENTANGLED THE NOSE GEAR CAME DOWN AND LOCKED AND THE NOSE GEAR LIGHT WAS ON. SINCE THE PILOT DID NOT HAVE AN INDICATION AND THE TOWER THOUGHT IT LOOKED DOWN IT MUST HAVE BEEN NEARLY DOWN BUT NOT LOCKED. THE DRAG BRACE MECHANISM WAS REMOVED AND NOTED THE DRAG BRACE SHAFT SHOWED SIGNS OF WEAR.
AFTER LOWERING THE LANDING GEAR, THE NOSE GEAR LIGHT DID NOT COME ON. A FLY BY WAS DONE AND THE TOWER THOUGHT THE GEAR LOOKED DOWN. THE ACFT LANDED NORMALLY BUT WHEN TAXIING OFF THE RUNWAY THE NOSE GEAR RETRACTED CAUSING THE NOSE TO SKID ON THE GROUND. THIS CAUSED THE NOSE GEAR TO ENTANGLE IN THE NOSE GEAR DOORS BENDING THEM AND BREAKING LINKAGE. AT THE SIGHT THE NOSE GEAR CAME DOWN AND LOCKED NORMALLY ONCE THE GEAR DOORS WERE OUT OF THE WAY. SINCE THERE WAS NO LIGHT, THE NOSE GEAR COULD NOT HAVE BEEN FULLY DOWN. AFTER FURTHER INSP THE DRAG BRACE SHAFT WAS FOUND TO HAVE WEAR AND SOME CORROSION ALTHOUGH IT STILL OPERATED FREELY.
LT ENG STARTED LOSING RPM. PILOT REPORTED FUEL PRESSURE DROPPED BELOW NORMAL RANGE BUT HAVE TO BELIEVE IT WAS OIL PRESSURE. ENG WAS CAGED AND LANDED SAFELY. THE OIL PRESSURE SCREEN WAS FULL OF ALUMINUM RESTRICTING OIL FLOW TO THE ENG. ON TEARDOWN, THE NR 4 CYL WRIST PIN PLUG WAS BALLED UP TO ABOUT HALF ITS NORMAL SIZE AND THE REMAINING METAL WAS FLUSHED THRU THE ENG AND INTO THE OIL SCREENS.
THE PILOT WAS UNABLE TO RETARD THE RT THROTTLE TO SLOW DOWN ON DESCENT FOR LANDING. SHUTDOWN AND FEATHERED ENG. WAS UNABLE TO TAXI ALL THE WAY INTO THE RAMP DUE TO DIFFICULTY STEERING WITH ONLY ONE ENG. RT MAGNETO COOLING FITTING PN 2610338 CAME OUT OF THE NW22WS-4-52-4 COOLING HOSE AND FELL DOWN BEHIND THE THROTTLE BELLCRANK ON THE FIREWALL. THIS WOULD NOT ALLOW FOR THE THROTTLE TO BE RETARDED. THE FITTING WAS REINSTALLED AND ACFT RETURNED TO SERVICE.
NOSE TIRE WENT FLAT ON LANDING. THE PILOT FELT THE NOSE GO FLAT ON ROLL OUT. HE HELD PRESSURE OFF UNTIL HE GOT AS SLOW AS POSSIBLE AND STOPPED ON THE RUNWAY. MX PERSONNEL CAME OUT AND REPLACED THE NOSE WHEEL ASSY AND THE PILOT TAXIED TO THE RAMP. AFTER DISASSEMBLY OF THE WHEEL, THE NOSE TUBE HAD 2.2500 INCH TO .1250 INCH SPLITS IN THE TREAD AREA LINED UP IN WHAT APPEARS TO BE A SEAM OR MOLD LINE. BOTH SPLITS WERE WITHIN 2 INCHES OF EACH OTHER.
LEFT ENGINE PILOT NOTICED PARTIAL POWER LOSS. AFTER LANDING THERE WAS A LARGE OIL LEAK FROM THE NR 6 EXHAUST PUSHROD TUBE WHICH HAD BEEN JARRED LOOSE AND UNCLIPPED. THE CAM FOLLOWER WAS BROKEN. THE TANG ON THE ROCKER COVER THAT HOLDS THE EXHAUST ROCKER SHAFT IN WAS BROKEN POSSIBLY LODGING IN THE VALVE SPRING CAUSE EXCESSIVE VALVE LASH.
THE HOLD DOWN STUDS ON NR 2 CYLINDER BROKE CAUSING ON OIL LEAK TO LOSS OIL PRESSURE.
PILOT REPORTED A VIOLENT NOSE SHIMMY ON LANDING. THE LINK STUD ON THE SPACER ASSEMBLY P/N ES10119 HAD BROKEN CAUSING THE STEERING ACTUATOR TO NO LONGER BE ATTACHED TO THE NOSE COLLAR.
THE RT ENGINE EXPERIENCED A LOSS OF POWER AND INDICATED A SIGNIFICANT INCREASE IN FUEL FLOW. THE ENGINE WAS SHUTDOWN AND A THE AIRCRAFT LANDED AT THE NEXT AVAILABLE AIRPORT. MAINTENANCE REVEALED THAT THE RETURN TO TANK LINE FROM THE FUEL FLOW DIVIDER WAS LOOSE AND LEAKING. THIS WOULD CAUSE A MASSIVE INCREASE IN FUEL FLOW. IT WAS A RELATIVELY LOW TIME INSTALLATION AND POSSIBLY SOME TWIST IN THE LINE CAUSED IT TO BACKOFF.
FLIGHT 5174 - EN ROUTE CID-CVG RECEIVED A FLAP FAIL CAUTION MESSAGE, CREW DECLARED AN EMERGENCY AND FLIGHT LANDED WITHOUT INCIDENT. REMOVED ICE BETWEEN THE LEFT AND RIGHT INBOARD FLAP LEADING EDGE AND THE MOVEABLE VANE.
LEFT VACUUM PUMP LOOSENED FROM ENGINE AND CAUSED A LOOSE OF OIL PRESSURE. THE VACUUM PUMP DRIVE WAS DAMAGED IN THAT THE GEAR WAS ROUNDED OFF. IT WAS HARD TO DETERMINE IF THE GEAR WORE AND CREATED STRESS TO WORK IT LOOSE FROM THE ENGINE OR IT WORKED LOOSE AND THEN DAMAGED THE GEAR.
FLIGHT 5164 - UPON REACHING FLIGHT LEVEL 330 DISPLAY COOL CAUTION MESSAGE APPEARED. AIRCRAFT DIVERTED TO GSO AND LANDED WITHOUT INCIDENT. REMOVED AND REPLACED FLOW SENSOR.
NOSE TIRE WAS FLAT ON LANDING. PILOT HAD SHIMMY AND VIBRATION ON ROLL-OUT. IN TRYING TO TAXI OFF THE RUNWAY, THE TIRE ROLLED OFF THE RIM AND BROKE THE NOSE WHEEL ASSEMBLY. THE NOSE WHEEL AND TIRE ASSEMBLY WAS REPLACE AND AIRCRAFT PUT BACK IN SERVICE.
FLIGHT 5457 - EN ROUTE JFK TO BUF CAPTAIN`S WINDSHIELD CRACKED. AIRCRAFT LANDED WITHOUT INCIDENT. REMOVED AND REPLACED LEFT WINDSHIELD.
LEFT ENGINE WAS LOSING RPM. WHEN RPM GOT BELOW 2000 THE PILOT FEATHERED THE ENGINE AND LANDED SAFELY. AT ENGINE TEAR DOWN THE NR 5 CYLINDER EXHAUST SEAT HAD COME LOOSE IN THE HEAD AND CAUSE ALUMINUM SHAVINGS TO GET IN THE OIL SYSTEM AND BLOCK THE PROP GOVERNOR. PROBABLE CAUSE WAS A SUDDEN COOL DOWN OF THE ENGINE AT SOME POINT.
FLIGHT 9479 - EN ROUTE CVG-MHT RECEIVED A DISPLAY COOL MESSAGE, FLIGHT DIVERTED TO PIT. REPLACED CLOGGED AIR FILTER FOR THE ELECTRONIC FLIGHT INSTRUMENT SYSTEM.
NOSE GEAR WOULD NOT COME DOWN AND LOCK ALL THE WAY. NOSE GEAR DOWN LIGHT WAS NOT ON. RETRACT ACTUATOR WAS BROKEN AT TOP END AND INTERFERED WITH DRAG BRACE MOVEMENT.
METAL CONTAMINATION IN OIL SCREEN DURING INSPECTION. REMOVED ALL CYLINDERS AND RODS AND FOUND 2 ROD BEARINGS FLAKING METAL OFF. THESE 2 BEARINGS AND ONE OTHER WERE NOT THE NEWEST PART NUMBER AS CURRENTLY SUPPLIED BY SUPERIOR. THEY WERE REPLACED AND ENGINE RETURNED TO SERVICE.
FLIGHT 5745 - DURING BTV APPROACH RECEIVED A FLAP FAIL CAUTION MESSAGE AT ZERO DEGREES, CREW DECLARED AN EMERGENCY AND FLIGHT LANDED WITHOUT INCIDENT. COMPLIED WITH AD 98-20-01 FLAP CAUTION MESSAGE -FIRST EVENT- MAINTENANCE ACTION, PARAGRAPH (B) 1, 2, 3, (A, B, C AND E). FLAP SYSTEM WAS RESET WITH NO FURTHER FLAP CAUTION MESSAGES.
FLIGHT 5686 - DURING OPERATION OF FLAPS WHILE AT THE GATE RECEIVED A FLAP FAIL CAUTION MESSAGE. REPLACED THE RIGHT BRAKE POSITION SENSING UNIT.
RT ENGINE HAD NO RPM CONTROL TAKING OFF. PROPELLER DID NOT FEATHER WHEN FEATHER WAS SELECTED. AC LANDED SAFELY AND FEATHER AFTER SHUTDOWN. TEARDOWN OF ENGINE THE FRONT END OF THE CAMSHAFT WAS BROKEN WHERE THE PROP GOVERNOR DRIVE GEAR ATTACHES. (K)
PILOT REPORTED LT ENGINE QUIT ON SHORT FINAL. ENGINE FEATHERED ITSELF AND LANDED SAFELY. THE CRANKSHAFT AND CRANKCASE HAD BROKEN BETWEEN NR 4 AND NR 5 CYLINDER. THIS REAR PART OF THE ENGINE WAS SEPARATED FROM THE REST OF THE ENGINE. (K)
FLIGHT 5673- ANTI ICE DUCT WARNING. REPLACED THE LT FUSELAGE SENSING ELEMENT A47WK.
CRANKCASE, LARGE CRACK UNDER NR 2 CYLINDER, RESULTING IN MASIVE OIL LOSS. (K)
RT ENGINE OIL QUANTY ZERO, OIL PRESSURE LOW (24-28 PSI). ENGINE WAS SHUT DOWN. ENGINE WINDMILLED 63 MIN W/ APPROX 12 PSI. OIL TEMP 100 DEGREES AT SHUTDOWN. REPLACED CRACKED OIL LINE. LEAK CHECKS GOOD.
ENGINE LOST POWER DUE TO LOSS OF OIL. ENGINE WAS CAGED IN OMA AND LANDED SAFELY. GROUND INSPECTION SHOWED HOLE IN CRANKCASE. PROBABLY ROD CAP SEPARATION DUE TO ROD BEARING FAILURE.
NR 5 CYLINDER WRIST PIN CAP ROLLED UP IN PISTON. CAUSE METAL FRAGMENTS IN OIL SCREEN. RESTRICTED OIL FLOW TO GOVERNOR. CAUSED DROP IN RPM. ENGINE WAS FEATHERED AND LANDED SAFETY.
NR 1 CYLINDER BARREL BROKE CAUSING PISTON TO BE CAUGHT ON THE DOWN STROKE. THEN ROD BOLTS BROKE AND ROD CAP CAME OFF. ENGINE LOST MUCH OF OIL AND WAS FEATHERED AND LANDED SAFELY.
FLIGHT 5450 DURING CRUISE FLIGHT RECEIVED A HYDRAULIC SYSTEM NR 2 LOW PRESSURE WARNING. CREW DECLARED AN EMERGENCY AND DIVERTED TO TYS. REPLACED FAILED NR 2 ENGINE DRIVEN HYDRAULIC PUMP.
FOUND R1 DOOR WILL NOT ARM. REMOVED DEBRIS FROM UNDERNEATH GIRT BAR. SLIDE ENGAGE OPS NORMAL. (M)
UNABLE TO DISARM DOOR 1R. FOUND ROPE/LANYARD TO BE INPROPERLY STOWED ON SLIDE AND WAS INTERFERING WITH THE GIRT BAR. STOWED ROPE/LANYARD PROPERLY, AND OPS CHECKED PER AMM 52-11-25. OPS CHECK NORMAL. (M)
FLIGHT 5921 HYDRAULIC SYSTEM 3 LOW PRESSURE CAUTION AND GEAR DISAGREE WARNING. REPLACED SYSTEM 3A HYDRAULIC PUMP.
FLIGHT 5158 RECEIVED A FLAP FAIL CAUTION MESSAGE DURING CLIMBOUT OF CVG. CREW DECLARED AN EMERGENCY AND RETURNED TO THE FIELD. COMPLIED WITH AD 98-20-01 FLAP CAUTION MESSAGE FIRST EVENT MAINTENANCE ACTION, PARAGRAPH (B) 1, 2, 3 (A, B, C AND E). FLAP SYSTEM WAS RESET WITH NO FURTHER FLAP CAUTION MESSAGE.
FLIGHT 5803 ANTI ICE DUCT WARNING. REPLACED BLEED LEAK SENSING ELEMENT.
FLIGHT 5201 LEFT ANTI ICE DUCT WARNING. COULD NOT DUPLICATE. INSPECTED SYSTEM AND FOUND NO DEFECTS.
EGRESS FLOOR LIGHTS BETWEEN ROW 5 TO ROW 9 INOPERATIVE. REMOVED AND REPLACED NR 731 BATTERY PACK AND POWR SUPPLY EGRESS LIGHTS, OP'S CHECK NORMAL. (M)
L1 DOOR SLIDE LIGHT INOPERATIVE. REMOVED AND REPLACED BATTERY PACK NR 731 POWRER SUPPLY IAW MM 33-51-07. OPS CHECK NORMAL. (M)
EICAS MSG ENGINE VIB DISPLAYED, INTERMITTENLY CAME ON IN CLIMB, WENT OUT IN CRUISE FAILED TO .1 CAME BACK 1.0-1.1. T/S PER FIM 77-31-00. REMOVED AND REPLACED AVM SYSTEM IAW M/M 77-31-00. (M)
EICAS STATUS MSG LEFT ENGINE FIRE LOOP NR 1 DISPLAYED. DEFERRED PER MEL 26-11-1. (M)
LT ENGINE FIRE LP-1 DISPLAYED. RERACKED AFOLTS CARD IAW FIM 26-11-00. RERACKED IAW AMM 26-10-01. OK FOR SERVICE. (M)
ON DESCENT, LT EEC AND LT ENG LIMITER INOP LIGHTS ILLUMINATED. EICAS MSG LT ENG EEC AND LT ENG LIMITER DISPLAYED. ON ENGINE START STARTER DID NOT DISENGAGE AT 49 PERCENT. BIT BVCU FOUND CODE 06, REPLACED PCCU. ENGINE START AND OPS SATIS MM 73-21-10-4. (M)
LEFT ENGINE FIRE LP 1. PERFORMED FIM PROCEDURE 26-11-00, OPS CHECK NORMAL. (M)
RIGHT MAIN GEAR GREEN LIGHT INOPERATIVE. REPLACD RIGHT MLG LAMP ASSEMBLY PER CHAPTER 20 PART USED WAS CCN 3221420. (M)
CRACK NOTED AT FLANGE RADIUS OF LT FRAME AT FS 718. REPARIED IAW SB 601R-53-055 PART B IAW EA NR 10-5320-00242.
LT ENGINE WOULD NOT REACH TO EPR WITH EEC AND ENG LIMITER ON. ENG PARAMETERS NORM FOR LOW EPR TO WITH EE C AND ENG LIMITER OFF NOT CHECKED. REMOVED AND REPLACED NR 1 ENG FFG IAW MM. REF DIS 7100-482 AND -483 FOR LEAK CHECK AND POWER PLANT ADJUSTMENT TEST.
Linked aircraft
| N-number | Make / model | Year | Status | Link basis |
|---|---|---|---|---|
| N107DF | — | — | Matched by certificate designator | |
| N107DF | — | — | Operator named in NTSB report | |
| N118PW | AERO COMMANDER 500-B | 1964 | Valid Registration | Operator named in NTSB report |
| N118PW | AERO COMMANDER 500-B | 1964 | Valid Registration | Matched by certificate designator |
| N127KH | AERO COMMANDER 500-B | 1961 | Valid Registration | Matched by certificate designator |
| N131JT | AERO COMMANDER 500-B | 1964 | Valid Registration | Matched by certificate designator |
| N23BQ | AERO COMMANDER 500-B | 1961 | Valid Registration | Matched by certificate designator |
| N261ER | AERO COMMANDER 500-B | 1963 | Valid Registration | Matched by certificate designator |
| N272CA | AERO COMMANDER 500-B | 1964 | Valid Registration | Matched by certificate designator |
| N304JT | AERO COMMANDER 500-B | 1965 | Valid Registration | Matched by certificate designator |
| N30MB | — | — | Operator named in NTSB report | |
| N324RR | AERO COMMANDER 500-B | 1964 | Valid Registration | Matched by certificate designator |
| N411ET | AERO COMMANDER 500-B | 1966 | Valid Registration | Matched by certificate designator |
| N411JF | AERO COMMANDER 500-B | — | Valid Registration | Matched by certificate designator |
| N411PT | AERO COMMANDER 500-B | 1962 | Valid Registration | Matched by certificate designator |
| N415BH | AERO COMMANDER 500-B | 1960 | Valid Registration | Matched by certificate designator |
| N443WA | AERO COMMANDER 500-B | 1963 | Valid Registration | Matched by certificate designator |
| N444CA | AERO COMMANDER 500-B | 1964 | Valid Registration | Operator named in NTSB report |
| N444CA | AERO COMMANDER 500-B | 1964 | Valid Registration | Matched by certificate designator |
| N444CB | AERO COMMANDER 500-B | 1961 | Valid Registration | Matched by certificate designator |
| N446AE | AERO COMMANDER 500-B | 1966 | Valid Registration | Matched by certificate designator |
| N516DT | AERO COMMANDER 500-B | 1965 | Valid Registration | Operator named in NTSB report |
| N516DT | AERO COMMANDER 500-B | 1965 | Valid Registration | Matched by certificate designator |
| N523AT | AERO COMMANDER 500-B | 1962 | Valid Registration | Matched by certificate designator |
| N524HW | — | — | Operator named in NTSB report | |
| N607MM | AERO COMMANDER 500-U | 1967 | Valid Registration | Matched by certificate designator |
| N610BW | AERO COMMANDER 500-B | 1965 | Valid Registration | Matched by certificate designator |
| N615MT | AERO COMMANDER 500-B | 1960 | Valid Registration | Matched by certificate designator |
| N630KC | AERO COMMANDER 500-B | 1960 | Valid Registration | Matched by certificate designator |
| N690RR | AERO COMMANDER 500-B | 1962 | Valid Registration | Matched by certificate designator |
| N712AT | CIRRUS DESIGN CORP SR22 | 2017 | Valid Registration | Operator named in NTSB report |
| N713SP | AERO COMMANDER 500-B | 1964 | Valid Registration | Matched by certificate designator |
| N716TC | AERO COMMANDER 500-B | 1962 | Valid Registration | Matched by certificate designator |
| N719CA | GATES LEARJET CORP. 35A | 1979 | Valid Registration | Matched by certificate designator |
| N777CM | AERO COMMANDER 500-B | 1964 | Valid Registration | Matched by certificate designator |
| N818TE | AERO COMMANDER 500-B | 1960 | Valid Registration | Matched by certificate designator |
| N888CA | PIPER PA-46-310P | 1984 | Valid Registration | Operator named in NTSB report |
| N917GT | AERO COMMANDER 500-B | 1960 | Valid Registration | Operator named in NTSB report |
| N917GT | AERO COMMANDER 500-B | 1960 | Valid Registration | Matched by certificate designator |
| N922BS | AERO COMMANDER 500-B | 1966 | Valid Registration | Matched by certificate designator |