RICHMOR AVIATION, INC.

Part 135 operator · designator BQVA

Data confidence: All records on this page are linked by a shared certificate number or aircraft registration (N-number).

Also recorded as: RICHMOR AVIATION, INC., Richmor Aviation, Inc.

Accident & enforcement record

Events that happened, regardless of the operator's own reporting. Each links to its public source.

NTSB accidents & incidents

No NTSB accidents or incidents linked to this operator.

FAA enforcement actions

FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.

Maintenance disclosure history

Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.

47 reports on file.

O · 2019-05-01 Matched by certificate designator
N939GP · ATA 2742

SDR SUBMISSION NOT REQUIRED BUT IMPORTANT ISSUE SO DID. AD 2014-21-06 ADDRESSES FAILURE OF HORIZONTAL STABILIZER ACTUATOR ACME NUT THREADS. REPETITIVE REPLACEMENT OF THE ACTUATOR ACME NUT AND JACK SCREW IS REQUIRED PER THE AD "REPEAT THE REPLACEMENT THEREAFTER AT INTERVALS NOT TO EXCEED 1,800 FLIGHT HOURS, OR AT EVERY PTA OVERHAUL, WHICHEVER OCCURS FIRST". FOUND ACTUATOR FROM THIS AIRCRAFT WITH EXCESSIVE PLAY AT THE ACME NUT THREADS. THREADED NUT TO DIFFERENT LOCATION ON JACK SCREW WITH EXCESSIVE PLAY STILL PRESENT. ACTUATOR HAD 417 HOURS & 330 LANDING SINCE LAST JACK SCREW & ACME NUT REPLACEMENT PER AD. ACME NUT WAS EXCESSIVELY WORN AFTER ONLY ACCRUING 23% OF THE ALLOWED INTERVAL. PERIODIC LUBRICATION OCCURS AS REQUIRED BY BEECH.

Source: SDR BQVA2019050800001 · FAA SDRS
B · 2018-08-16 Matched by certificate designator
N200FR · ATA 2750

AIRCRAFT LANDED & FLAPS WERE RETRACTED. TAXIED TO FBO. AIRCRAFT WAS TAXIED IN PREPARATION FOR DEPARTURE. WITH AIRCRAFT STILL ON GROUND, AN ODOR WAS NOTICED BY CREW. AIRCRAFT RETURNED TO FBO. SOME SIGNS OF SMOKE WERE VISIBLE BUT NO FURTHER ISSUE. IDETERMINED THAT POWER WAS STILL APPLIED TO THE FLAP MOTOR WITH FLAPS FULLY RETRACTED. PROBLEM WAS DEFECTIVE FLAP UP LIMIT SWITCH. AFTER TROUBLESHOOTING AND INSPECTION, SWITCH & FLAP MOTOR WERE REPLACED. OPS CHECKED OK.

Source: SDR BQVA201808170016 · FAA SDRS
O · 2018-06-12 Matched by certificate designator
N119FM · ATA 5520

DURING INSPECTION, SIGNS OF RUST WERE DETECTED ON THE HORIZONTAL STABILIZER AFT PIVOT BUSHINGS, ON THE LEFT AND RIGHT SIDES. PIVOT BOLTS AND BEARING WAS REPLACEED.

Source: SDR BQVA2018061400201 · FAA SDRS
O · 2018-06-01 Matched by certificate designator
N119FM · ATA 5330

DURING COMPLIANCE OF CMP CODE 532085, THE LEFT AND RIGHT OVERWING AREAS BETWEEN THE DRAG BEAM AND WING TO BODY FAIRING, BS 257.5 - 512, FUSELAGE SKIN CORROSION WAS FOUND WHERE AFT WING ROOT MEETS THE FUSELAGE, STRINGERS 23 LT AND RT, BS 498-526.

Source: SDR BQVA2018060500001 · FAA SDRS
K · 2017-10-01 Matched by certificate designator
N689BV · ATA 3240

LOSS OF LEFT BRAKE PRESSURE FROM BOTH THE PILOT & COPILOT POSITIONS. AMPLE RUNWAY WAS AVAILABLE TO STOP SAFELY USING PROP REVERSE.

Source: SDR BQVA201710050001 · FAA SDRS
J · 2015-09-29 Matched by certificate designator
N689BV · ATA 7200

RIGHT CHIP DETECTOR ANNUNCIATOR ILLUMINATED INTERMITTENTLY. DURING FINAL WITH THE RT CHIP DETECTOR ANNUNCIATOR EXTINGUISHED, CREW REDUCED POWER FOR LANDING. ONCE THE POWER WAS REDUCED FAR ENOUGH, THE RT OIL PRESS WAS OBSERVED TO BE LOWER THAN USUAL, BUT STILL WITHIN THE NORMAL OPERATING RANGE. MX WAS DISPATCHED TO ACFT. ENG CHANGE IN PROGRESS.

Source: SDR BQVA20150929001 · FAA SDRS
J · 2015-04-17 Matched by certificate designator
N300FJ · ATA 3240

PRIOR TO LANDING THE BRAKE FAIL CAS MSG ILLUMINATED. AFM PROCEDURES WERE FOLLOWED FOR LANDING. TROUBLE SHOT & REPLACED THE BRAKE COMMAND MODULE.

Source: SDR BQVA20150417001 · FAA SDRS
O · 2015-01-29 Matched by certificate designator
N300FJ · ATA 2710

LEFT WING AILERON CABLE CHAFING AT OTBD BELL CRANK.

Source: SDR BQVA20150129001 · FAA SDRS
J · 2015-01-09 Matched by certificate designator
N58AJ · ATA 2420

LEFT AC & LEFT DC POWER FAIL INDICATORS ILLUMINATED.

Source: SDR BQVA20150109001 · FAA SDRS
O · 2014-04-21 Matched by certificate designator
N58AJ · ATA 5711

DURING COMPLIANCE OF CMP CODE 279010 LT AILERON HINGE INSPECTION, A SMALL AREA OF CORROSION WAS FOUND ON THE WING AFT LOWER SPAR CAP JUST OTBD OF THE CTR AILERON HINGE.

Source: SDR BQVA20140425001 · FAA SDRS
O · 2013-12-11 Matched by certificate designator
N58AJ · ATA 5247

DURING COMPLIANCE OF FUSELAGE EXTERIOR INSPECTION, CMP CODE 531020, FOUND CORROSION AT APU EXHAUST OPENING. STANDARD REPAIR APU DOOR SKIN FS 617.562 CURRENTLY IN PROGRESS.

Source: SDR BQVA20131211001 · FAA SDRS
O · 2013-05-03 Matched by certificate designator
N57MH · ATA 5210

CABIN DOOR WAS REMOVED AND SENT TO REPAIR FACILITY FOR COMPLIANCE OF BOMBARDIER SERVICE BULLETIN 601-0613 R1. THE FOLLOWING ITEMS WERE FOUND WITH CORROSION DURING SERVICE BULLETIN COMPLIANCE: AFT SUPPORT ANGLE P/N 600-31902-65 LOWER END, ATTACH CLIP P/N 600-31902-54 AT STA 329.06, ATTACH CLIPS P/N 600-31902-53 AND 600-31902-54 AT STA 320.10, AND ATTACH CLIP P/N 600-31902-54 AT STA 338.

Source: SDR BQVA20130507001 · FAA SDRS
B · 2012-04-16 Matched by certificate designator
N55422 · ATA 3340

ON CLIMB-OUT, CREW NOTICED SMOKE EMANATING FROM ABOVE AND BELOW INSTRUMENT PANEL. ATC WAS NOTIFIED, THE MASTER SWITCH WAS TURNED OFF, AND THEY RETURNED TO DEPARTURE. FIRE/ RESCUE PERSONNEL VERIFIED THERE WAS NO ACTIVE FIRE. THE ACFT WAS TURNED OVER TO MX FOR INSP AND REPAIR. MX PERSONNEL DETERMINED THAT THE PROBLEM WAS WITH THE LANDING LIGHT SWITCH. THE LANDING LIGHT SWITCH WAS REPLACED WITH A CURRENT PART NUMBERED SWITCH. AN OPS CHECK WAS PERFORMED WITH NO DIFFICULTIES NOTED.

Source: SDR BQVD2012041600000 · FAA SDRS
O · 2011-12-14 Matched by certificate designator
N300FJ · ATA 3240

BRAKE FAIL CAS MESSAGE ON SHORT FINAL - NO NORMAL BRAKING ON LANDING ROLL. EMERGENCY BRAKE SYSTEM UTILIZED SUCCESSFULLY WITHOUT INCIDENT.

Source: SDR BQVA20111219 · FAA SDRS
O · 2011-06-08 Matched by certificate designator
N227SV · ATA 5720

DURING COMPLIANCE OF CMP CODES 573013 & 573014 WINGLET ATTACH HARDWARE (LEFT & RIGHT) - INSPECTION, SOME CORROSION WAS FOUND IN THE WINGLET ATTACH BORES ONCE THE BUSHINGS WERE REMOVED.

Source: SDR BQVA2011061300010 · FAA SDRS
O · 2011-04-15 Matched by certificate designator
N58AJ · ATA 5730

DURING COMPLIANCE OF CMP CODES 576511 & 576516 WINGLET ATTACH HARDWARE (LEFT & RIGHT) - INSPECTION (144 MONTH), SOME CORROSION WAS FOUND IN THE WINGLET ATTACH BORES ONCE THE BUSHINGS WERE REMOVED.

Source: SDR BQVA2011041900009 · FAA SDRS
O · 2011-03-15 Matched by certificate designator
N540EA · ATA 5713

SURFACE CORROSION WAS DETECTED ON THE HORIZONTAL FLANGES OF STRINGER 8 ON BOTH THE LEFT AND RIGHT CONNECTING ANGLES.

Source: SDR BQVA201103210009 · FAA SDRS
O · 2011-03-09 Matched by certificate designator
N540EA · ATA 5313

SURFACE CORROSION FOUND ON STRINGER 24L AND SOME CORROSION FOUND ON THE SHIM DURING THE FS 580 BULKHEAD COMSCAN INSPECTION (CMP CODE 539435). (ORIGINAL SUBMISSION 3/14/11)

Source: SDR BQVA2011031400008 · FAA SDRS
O · 2010-08-18 Matched by certificate designator
N50BH · ATA 5312

SUSPECTED CORROSION FOUND DURING INSPECTION OF THE FS 580 BULKHEAD SKIN SPLICE, AREA LONGERONS AND STRINGERS 24 L/R IN ACCORDANCE WITH CMP 539540. AFTER FURTHER NDT THE AREA WAS FOUND TO HAVE MINOR SURFACE CORROSION WHICH WAS REMOVED AND TREATED. FINDINGS WERE SUBMITTED TO ENGINEERING REF WO CS217760, AND FOUND TO BE ACCEPTABLE FOR RETURN TO NORMAL OPERATIONS WITHOUT RESTRICTIONS.

Source: SDR BQVA2010082300007 · FAA SDRS
O · 2010-04-07 Matched by certificate designator
N58AJ · ATA 5340

DURING THE REQUIRED EDDY CURRENT INSPECTION OF THE FS 793 BULKHEAD CAP ANGLE, CRACKS WERE FOUND AROUND LEFT AND RIGHT BOLT HOLES IN THE CAP ANGLE FOR THE VERTICAL FIN ATTACHMENT.

Source: SDR BQVA2010040900005 · FAA SDRS
O · 2010-04-07 Matched by certificate designator
N58AJ · ATA 5730

DURING A WING NDT INSPECTION OF THE LT WING PLANK AT FS 452 BL 33, CORROSION WAS FOUND. ENGINEERING HAS DETERMINED THIS CORROSION IS EXCESSIVE ENOUGH TO REQUIRE ACCOMPLISHMENT OF ASC 229, WHICH WILL REMOVE THE CORROSION ON THE PLANK AND INSTALL A THREE PIECE FITTING PLATE.

Source: SDR BQVA2010041200006 · FAA SDRS
N · 2010-02-23 Matched by certificate designator
N58AJ · ATA 3260

AIRCRAFT DEPARTED FROM KHPN EN ROUTE TO KFPR. CREW SELECTED GEAR HANDLE DOWN AND RECEIVED A RED HANDLE WARNING INDICATION. AIRCRAFT FLEW PAST CONTROL TOWER TO VERIFY THE LANDING GEAR WAS DOWN. RETRACTED LANDING GEAR AND DIVERTED TO KPBI AND LANDED WITH OUT INCIDENT. AIRCRAFT WAS BROUGHT TO GENERAL DYNAMICS WHERE THE LEFT MAIN LANDING GEAR DOWN AND LOCKED SWITCH WAS REPLACED.

Source: SDR BQVA2010030100005 · FAA SDRS
O · 2010-01-02 Matched by certificate designator
N50BH · ATA 5610

RIGHT SIDE WINDSHIELD OUTER PANE FAILURE DURING FLIGHT. REMOVED AND REPLACED WINDSHIELD.

Source: SDR BQVA2010010400004 · FAA SDRS
O · 2009-07-13 Matched by certificate designator
N689BV · ATA 3240

RIGHT HAND BRAKE PEDAL LOST PRESSURE INITIALLY THEN REGAINED AFTER ACTUATING BRAKES. NO COMPONENT DEFECT. REMOVED TRAPED AIR IN BRAKING SYSTEM.

Source: SDR BQVA2009071300003 · FAA SDRS
N · 2009-06-15 Matched by certificate designator
N205EL · ATA 3260

INTERNAL FAILURE OF LT LANDING GEAR DOWNLOCK SENSOR WHICH IS PART OF THE LT LANDING GEAR SIDE BRACE ACTUATOR.

Source: SDR BQVA2009061500002 · FAA SDRS
J · 2009-03-16 Matched by certificate designator
N797CM · ATA 7930

NR 2 ENGINE OIL PRESSURE AT BOTTOM OF GREEN ARC ON GAUGE, 60 PSI.

Source: SDR BQVA2009031600001 · FAA SDRS
K · 2008-07-01 Matched by certificate designator
N689BV · ATA 3240

UPON TAXI OUT AT AIRCRAFT LOST BRAKING ON RT MLG. THE AIRCRAFT WAS BROUGHT TO MAINTENANCE SEALS ON THE RT BRAKE ASSY WERE REPLACED SYS WAS BLEED AND SERVICED WITH FLUID. NO DEFECTS NOTED; AIRCRAFT WAS RETURNED TO SERVICE. (K)

Source: SDR BQV2008F00000 · FAA SDRS
J · 2007-06-05 Matched by certificate designator
N205EL · ATA 3233

DURING FINAL APPROACH TO TUCSON, AZ (TUS) WHEN THE LANDING GEAR WAS SELECTED DOWN AN UNSAFE INDICATION WAS ILLUMINATED FOR THE LEFT MAIN POSITION. DURING THREE ATTEMPTS THE UNSAFE INDICATION REMAINED AND AFM ABNORMAL PROCEDURES FOR GEAR EXTENSION WERE FOLLOWED; THE UNSAFE INDICATION REMAINED. THE AIRCRAFT MADE A LOW PASS BY THE TOWER TO VERIFY GEAR DOWN, AN EMERGENCY WAS DECLARED AND THE AIRCRAFT LANDED WITHOUT INCIDENT; PROCEDING TO MAINTENANCE AT LEARJET. THE LT DRAG STAY ACTUATOR WAS REPLACED AND THE LANDING GEAR WAS CYCLED 4 TIMES ON JACKS WITH NO DEFECTS; THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR BQVA200766071 · FAA SDRS
O · 2007-05-18 Matched by certificate designator
N50BH · ATA 5740

WING TO FUSELAGE ATTACH FITTING AT FS 452 BL 33 (LEFT SIDE), CORROSION DETECTED DURING THE SCHEDULED ULTRASONIC INSPECTION. THE CORROSION ON THE OUTBOARD SURFACE IS .158 INCH IN DEPTH, .125 INCH IN LENGTH; AND .125 INCH IN DIAMETER. [07-03-07] ENGINEERING HAS GRANTED A FLIGHT ALLOWANCE UNDER WO CS117819. THIS ALLOWS CONTINUED NORMAL OPERATION FOR 180 DAYS UNTIL NOV. 27, 2007 BY WHICH TIME A REPAIR IAW ASC229 WILL BE REQUIRED.

Source: SDR BQVA200752271 · FAA SDRS
O · 2007-05-16 Matched by certificate designator
N50BH · ATA 5340

DURING THE REQUIRED EDDY CURRENT INSPECTION OF THE FS 793 BULKHEAD CAP ANGLE, CRACK INDICATIONS WERE NOTED ON BOTH SIDES. THE CRACKS ARE ABOVE THE .5 INCH BOLT HOLES IN THE CAP ANGLE FOR VERTICAL FIN ATTACHMENT.

Source: SDR BQVA200751871 · FAA SDRS
O · 2007-02-01 Matched by certificate designator
N982RK · ATA 5730

DURING THE SCHEDULED 72 MONTH LT WING WEDGE INSPECTION CMP 575030, ONE WING WEDGE HOLD DOWN RIVNUT WAS FOUND TO BE IN AN OVERSIZED HOLE.

Source: SDR BQVA200721071 · FAA SDRS
B A · 2006-07-06 Matched by certificate designator
N50BH · ATA 2530

ON APPROACH FLIGHT CREW NOTICED AN ACRID SMELL, THE AIRCRAFT LANDED AND EXITED THE RUNWAY WITHOUT INCIDENT AT WHICH TIME SMOKE WAS SEEN IN THE AFT GALLEY AND THE OVER COUNTER LIGHT LENS HAD OBSERVABLE FLAMES. THE PILOT REMOVED ELECTRICAL POWER FROM THE GALLEY, AND THE CO-PILOT DISCHARGED THE AFT HALON EXTINGUISHER WHICH PUT OUT THE FIRE.

Source: SDR 7706 · FAA SDRS
B · 2006-07-06 Matched by certificate designator
N50BH · ATA 2120

ON APPROACH THE FLIGHT CREW NOTICED AN ACRID SMELL, THE AIRCRAFT LANDED AND EXITED THE RUNWAY WITHOUT INCIDENT AT WHICH TIME SMOKE WAS SEEN IN THE AFT GALLEY AND THE OVER COUNTER LIGHT LENS HAD OBSERVABLE FLAMES. THE PILOT REMOVED ELECTRICAL POWER FROM THE GALLEY, AND THE CO-PILOT DISCHARGED THE AFT HALON EXTINGUISHER WHICH PUT OUT THE FIRE.

Source: SDR BQVA200677061 · FAA SDRS
O · 2006-05-04 Matched by certificate designator
N205EL · ATA 5321

TWENTY FIVE SPOTS OF CORROSION FOUND ON THE CABIN SUB FLOOR AND DOUBLERS FROM 1 X 2 INCHES IN SIZE TO 1.5 X 9 INCHES IN SIZE AND FROM .002 TO .022 INCHES IN DEPTH EXTENDING DOWN THE RIGHT SIDE OF THE CABIN EXTENDING FROM FS 379 TO FS 559.

Source: SDR BQVA200655061 · FAA SDRS
P · 2006-03-19 Matched by certificate designator
N227SV · ATA 2130

LEFT BLEED AIR VALVE PBA SWITCH LAMP FAILURE, NO INDICATION OF CLOSED VALVE. RESULTED IN CABIN O2 MASK DEPLOYMENT WITH AIRCRAFT DIVERTED TO RALIEGH DURHAM, NC (RDU).

Source: SDR BQVA32306 · FAA SDRS
Z · 2006-03-16 Matched by certificate designator
N982RK · ATA 5345

DURING COMPLIANCE WITH CMP 532010 ENTRANCE COMPARTMENT BEHIND PANEL INSPECTION, THE MAIN CABIN DOOR ACTUATOR SUPPORT ASSEMBLY WAS FOUND CRACKED.

Source: SDR 3202006 · FAA SDRS
O · 2006-01-23 Matched by certificate designator
N50BH · ATA 5711

DURING MAINTENANCE, WHILE ACCOMPLISHING A SCHEDULED 72 MONTH INSPECTION, 5 PATCHES OF CORROSION WERE FOUND ON THE ON THE AFT SIDE OF THE RT WING REAR SPAR (BEAM WEB) BEHIND THE RAIN CURTAINS AT FASTENER LOCATIONS EXTENDING FROM RBS 359 TO 422. THE MEASURED CORROSION DEPTH RANGE WAS FROM .002 INCH TO .029 INCH AND ONE AREA MEASURING .058 INCH.

Source: SDR 23JAN2006 · FAA SDRS
O · 2006-01-05 Matched by certificate designator
N50BH · ATA 5711

DURING MAINTENANCE WHILE ACCOMPLISHING A SCHEDULED 72 MONTH INSPECTION, 8 PATCHES OF CORROSION WERE FOUND ON THE ON THE AFT SIDE OF THE LT WING REAR SPAR (BEAM WEB) BEHIND THE RAIN CURTAINS AT FASTENER LOCATIONS EXTENDING FROM RBS 340 TO 406. THE LARGEST PATCH OF CORROSION WAS MEASURED AT 2 INCHES X 4.5 INCHES, WITH A DEPTH RANGE FROM .002 INCH TO .029 INCH AND ONE AT .058 IN.

Source: SDR EA0123JAN2006 · FAA SDRS
O · 2006-01-05 Matched by certificate designator
N50BH · ATA 5711

DURING MAINTENANCE WHILE ACCOMPLISHING A SCHEDULED 72 MONTH INSPECTION, 8 PATCHES OF CORROSION WERE FOUND ON THE ON THE AFT SIDE OF THE LT WING REAR SPAR (BEAM WEB) BEHIND THE RAIN CURTAINS AT FASTENER LOCATIONS EXTENDING FROM RBS 340 TO 406. THE LARGEST PATCH OF CORROSION WAS MEASURED AT 2 INCHES X 4.5 INCHES, WITH A DEPTH RANGE FROM .002 INCH TO .029 INCH AND ONE AT .058 INCH.

Source: SDR EA01BQVA0106A · FAA SDRS
O · 2002-12-16 Matched by certificate designator
N85VM · ATA 5610

DURING APPROACH TO IAD CO-PILOT WINDSHIELD OUTER PANE DEVELOPED MULTIPLE CRACKS.

Source: SDR 2003F00096 · FAA SDRS
O · 2001-05-22 Matched by certificate designator
N57MH · ATA 3230

AS PART OF A SCHEDULED INSPECTION BEING PERFORMED, AN EMERGENCY EXTENSION CHECK OF THE LANDING GEAR WAS PERFORMED. NITROGEN WAS HEARD LEAKING FROM THE LEFT SIDE NOSE WHEEL WELL AREA. FURTHER TROUBLESHOOTING REVEALED THE NOSE LANDING GEAR UPLOCK ACTUATOR (PNEUMATIC) TO BE LEAKING BY THE PISTON SHAFT AREA. CONSIDERABLE CORROSION WAS FOUND INTERNALLY (PISTON SPRING & CYLINDER SHAFT AREA).

Source: SDR 2001F00006 · FAA SDRS
O · 2001-05-18 Matched by certificate designator
N50TG · ATA 5330

CORROSION IN AREA OF AFT FUSELAGE SKINS AT ACU EXHAUST OUTLETS. WATER ENTRAPMENT. REPAIRED UNDER BOMBARDIER REO NR 601-53-30-278.

Source: SDR 2001FA0000009 · FAA SDRS
Y · 1997-07-22 Matched by certificate designator
N689BV · ATA 7260

RIGHT HAND ENGINE SHUT DOWN IN-FLIGHT DURING DESCENT INTO 1B1 AS A RESULT OF A SHEARED DRIVE SHAFT (ACCESSORY GEARBOX).

Source: SDR 97ZZZX3995 · FAA SDRS
O · 1996-08-13 Matched by certificate designator
N3127R · ATA 5330

LOWER FUSELAGE SKIN WAS FOUND CHAFED FROM CONTACT WITH THE AFT NOSE LANDING GEAR DOOR. CHAFING OCCURRED WITH THE LANDING GEAR EXTENDED AND AIRLOADS INDUCED. FUSELAGE SKIN AREA CHAFED WAS FORWARD OF PRESSURE BULKHEAD (NON-PRESSURIZED AREA). DOOR, P/N 45A31615-11.

Source: SDR 96ZZZX4384 · FAA SDRS
O · 1995-03-30 Matched by certificate designator
N900DH · ATA 2434

BLACK STREAKS WERE NOTICED ON THE ENGINE COWLING BY MAINTENANCE PERSONNEL. FOUND THE DC GENERATOR TO HAVE PREMATURE BRUSH WEAR, WORN BEYOND LIMITS (NO WEAR MARK REMAINING - 100 PERCENT WORN). RECENT OVERHAUL BY REPAIR STATION, CAUSE OF WEAR NOT DETERMINED. BRUSH PART NUMBER NOT DETERMINED. SUSPECT DEFECTIVE BRUSH MATERIAL COMPOSITION OR IMPROPER INSTALLATION/MAINTENANCE OVERHAUL PROCEDURE.

Source: SDR 95ZZZX1920 · FAA SDRS
O · 1995-03-16 Matched by certificate designator
N900DH · ATA 2434

BLACK STREAKS WERE NOTICED ON THE ENGINE COWLING BY MAINTENANCE PERSONNEL. FOUND THE D. C. GENERATOR TO HAVE PREMATURE BRUSH WEAR, WORN BEYOND LIMITS (NO WEAR MARK REMAINING - 100 PERCENT WORN). RECENT OVERHAUL BY REPAIR STATION. CAUSE OF BRUSH WEAR COULD NOT BE DETERMINED. BRUSH PART NUMBER NOT DETERMINED. SUSPECT DEFECTIVE BRUSH MATERIAL COMPOSITION OR IMPROPER INSTALLATION/MAINTENANCE OVERHAUL PROCEDURE.

Source: SDR 95ZZZX1921 · FAA SDRS
R · 1995-02-21 Matched by certificate designator
N58JF · ATA 7530

ENGINE WOULD NOT DEVELOP TAKEOFF THRUST. BLEED VALVE STRAP FOUND FRACTURED. AN EVALUATION (CONDITION REPORT) INDICATES FAILURE DUE TO FLUTTER AND HIGH-CYCLE FATIGUE BROUGHT ABOUT BY EXCESSIVE LOADING OF ONE OR MORE BLEED VALVE SPHERICAL BEARINGS. THIS APPEARS TO BE AN ISOLATED INCIDENT. IMPROPER ADJUSTMENT DURING OVERHAUL MAY HAVE BEEN A FACTOR.

Source: SDR 95ZZZX1521 · FAA SDRS

Linked aircraft

N-numberMake / modelYearStatusLink basis
N200FRMatched by certificate designator
N205ELBOMBARDIER INC BD-700-1A112006Valid RegistrationMatched by certificate designator
N2194DJI AGRAS T50Valid RegistrationMatched by certificate designator
N58AJGULFSTREAM AEROSPACE GIV-X (G450)2010Valid RegistrationMatched by certificate designator
N592FCGULFSTREAM AEROSPACE GIV-X (G450)2008Valid RegistrationMatched by certificate designator