SKY LEASE I, LLC

Part 121 operator · designator WRNA

Data confidence: All records on this page are linked by a shared certificate number or aircraft registration (N-number).

Also recorded as: SKY LEASE I INC., SKY LEASE I, LLC, SKYLEASE CARGO, SKYLEASE I, LLC, TRADEWINDS, TRADEWINDS AIRLINES

Accident & enforcement record

Events that happened, regardless of the operator's own reporting. Each links to its public source.

NTSB accidents & incidents

No NTSB accidents or incidents linked to this operator.

FAA enforcement actions

FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.

Maintenance disclosure history

Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.

429 reports on file — showing most recent 50.

O · 2026-02-18 Matched by certificate designator
N903AR · ATA 5330

LOWER FUSELAGE CENTER WING FRONT SPAR AT STA. RBBL 127.50, LOWER PANEL CORROSION.

Source: SDR WRNA202603190001 · FAA SDRS
O · 2026-02-18 Matched by certificate designator
N903AR · ATA 5310

LOWER FUSELAGE AT LH AND RH FWD SPAR OF CENTER TANK AT STA. 987 (APROX), SHOWS CORROSION.

Source: SDR WRNA202603190002 · FAA SDRS
O · 2026-02-18 Matched by certificate designator
N903AR · ATA 5310

DURING INSPECTION OF AFT CARGO DOOR, FOUND FRAME PUNCTURE HOLE AND CRACK ON AFT SECTION OF CARGO DOOR SKIN.

Source: SDR WRNA202603190003 · FAA SDRS
O · 2024-09-04 Matched by certificate designator
N904AR · ATA 3242

DURING POST FLIGHT FOUND # 3 BRAKE TORQUE LIMITER BROKEN.

Source: SDR WRNA202409040687 · FAA SDRS
B · 2022-09-27 Matched by certificate designator
N903AR · ATA 2121

DURING T/O CLIMB , ELECTRICAL ODOR FOLLOWING BY " EE CLNG SUPP FAN" ON STATUS PAGE.-

Source: SDR WRNA202209290372 · FAA SDRS
J · 2019-01-31 Matched by certificate designator
N904AR · ATA 2100

1.DURING CLIMB +-29000, HEARD A LOUD NOISE LIKE AN EXPLOSION , SELECT ECS AND SAW BOTH OUTFLOW VALVES CLOSED BUT RATE OF CLIMB +-1700. CABIN ALT REACH +- 10000. THE EQUIPMENT COOLING WARNING LIGHT CAME ON. PERFORMED CABIN ALT (QRH) DESCENT TO 10000, BACK TO DEPARTURE.

Source: SDR WRNA2019021131001 · FAA SDRS
E M · 2016-11-03 Matched by certificate designator
N742WA · ATA 7250

ON CLIMB OUT DEPARTING KMIA NR 2 ENGINE EXPERIENCED HIGH EGT, THROTTLE RETARDED , MINUTES LATER LOUD NOISE WAS HEARD, EGT CLIMBED TO 777 DEGREES CELSIUS AND ENGINE SHUT DOWN PROCEDURE WAS ACCOMPLISHED, FUEL WAS DUMPED AND RTB KMIA. AFTER PARKING FOUND EXCESSIVE TURBINE BLADE DAMAGE.

Source: SDR 2016F00216 · FAA SDRS
K A J · 2016-09-01 Matched by certificate designator
N903AR · ATA 4940

AIRCRAFT WAS BEING PREPARED FOR DEPARTURE. APU WAS STARTED AND APPROXIMATELY 5 MINUTES LATER, THE APU FIRE INDICATION ACTIVATED AND THE FLIGHT CREW PULLED THE APU FIRE T-HANDLE. THE APU FIRE BOTTLE HAD ALREADY AUTOMATICALLY ACTIVATED. UPON INSPECTION OF THE APU AND ITS AREA WAS FOUND THAT THE STARTER HAD BROKEN LOOSE AT ITS MOUNTING AT THE APU. IT APPEARED THAT AS A RESULT OF THE STARTER'S MOVEMENT UPON BREAKING LOOSE, IT DAMAGED A FUEL LINE, WHICH CAUSED A FUEL LEAK, WHICH IN TURN CAUSED THE FIRE. THE FIRE WAS EXTINGUISHED BY THE FIRE SUPPRESSION SYSTEM. AS A RESULT OF THE FIRE, THE RT INBD ELEVATOR WAS DAMAGED, AS WELL AS BOTH OF THE APU LOWER ACCESS DOORS. THE APU DOORS WERE R & R, AS WAS THE RT INBD ELEVATOR. THE APU WAS DEACTIVATED AND DEFERRED, AND WILL BE R & R UPON THE AIRPLANE'S ARRIVAL. TROUBLESHOOTING IS CURRENTLY IN PROGRESS TO DETERMINE THE CAUSE OF THE STARTER FAILURE.

Source: SDR 2016F00180 · FAA SDRS
J · 2016-07-08 Matched by certificate designator
N903AR · ATA 2160

DURING CRUISE, UPPER CABIN AND ALL DECKS TEMPERATURE EXCEEDED 60 DEGREES C. RETURNED TO DEPARTURE. EMERGENCY NOT DECLARED. TROUBLESHOOTING FOUND A DEFECTIVE ZONE TEMPERATURE CONTROLLER. CONTROLLER WAS REMOVED AND REPLACED, OPERATIONAL SYSTEM CHECK SATISFACTORILY PERFORMED PER AMM 21-61-01 AND 21-61-00, AIRPLANE RETURNED TO SERVICE.

Source: SDR WRNA2016F00149 · FAA SDRS
K J · 2016-01-24 Matched by certificate designator
N986AR · ATA 2913

DURING FLIGHT, RECEIVED A LEVEL 2 ALERT HYDRAULIC SYSTEM 3 FAIL. ACFT DIVERTED AND LANDED SAFELY. PUMP CASE DRAIN LINE CRACKED LINE WAS REPLACED.

Source: SDR WRNA201601270004 · FAA SDRS
K J · 2016-01-22 Matched by certificate designator
N986AR · ATA 2910

30 MINUTES INTO FLIGHT HYDRAULIC SYSTEM 3 PRESENTS HYDRAULIC SYS 3, LEVEL 1 ALERT, FOLLOWED BY QUANTITY LOW, FOLLOWED BY HYD SYSTEM 3 FAIL. ACFT RETURNED TO DEPARTURE.

Source: SDR WRNA201601210004 · FAA SDRS
E · 2016-01-08 Matched by certificate designator
N950AR · ATA 5755

HIGH VIBRATION ON CLIMB CONTINUED FOR REMAINDER OF FLIGHT. FOUND RT WING NR 2 SPOILER DELAMINATED.

Source: SDR WRN2016F00000 · FAA SDRS
E · 2016-01-08 Matched by certificate designator
N950AR · ATA 2760

RETURNED TO DEPARTURE DUE TO HIGH STRUCTURE VIBRATION ON CLIMB PHASE PASSING 16,000 AND REMAINED FOR REST OF FLIGHT.

Source: SDR WRNA201601080003 · FAA SDRS
M J · 2015-11-18 Matched by certificate designator
N904AR · ATA 2121

AT TOP OF CLIMB ELECTRONIC EQUIPMENT COOLING GROUND EXHAUST VALVE FAIL MESSAGE. WHEN SWITCHED ELECTRONIC EQUIPMENT COOLING TO OVERRIDE POSITION, CONTINUED TO HAVE THE OVERHEAT PROBLEM CAUSING A RETURN TO DEPARTURE.

Source: SDR WRNA201511200002 · FAA SDRS
R · 2015-10-28 Matched by certificate designator
N742WA · ATA 7200

NR 1 ENGINE LOST POWER, ALL OF ITS PARAMETERS DISPLAYED IDLE ON ECIAS. POWER RECOVERED IMMEDIATELY. MINUTES LATER SAME ENGINE LOST POWER AGAIN DURING CLIMB OUT. ALL ENGINE PARAMETERS DISPLAYED IDLE ON ECIAS BUT THIS TIME POWER WAS NOT RECOVERED. ENGINE CHECKLIST PERFORMED BY CREW. ENGINE WAS SHUTDOWN IAW PROPER PROCEDURES. ACFT RETURNED TO DEPARTURE SAFELY.

Source: SDR WRNA201510290031 · FAA SDRS
R · 2015-10-28 Matched by certificate designator
N742WA · ATA 7200

DEPARTING NR 1 ENG LOST POWER, ALL OF ITS PARAMETERS DISPLAYED IDLE ON ECIAS. POWER RECOVERED IMMEDIATELY, MINUTES LATER SAME ENGINE LOST POWER AGAIN DURING CLIMB OUT. ALL ENGINE DISPLAYED IDLE ON ECIAS BUT THIS TIME POWER WAS NOT RECOVERED. ENGINE CHECKLIST PERFORMED BY CREW. ENGINE WAS SHUTDOWN IAW PROPER PROCEDURES. ACFT RETURNED TO DEPARTURE SAFELY.

Source: SDR WRNA201511280001 · FAA SDRS
R J · 2015-10-21 Matched by certificate designator
N986AR · ATA 7200

DURING APPLICATION OF TAKEOFF POWER, ENGINE NR 1 DID NOT ACCELERATE. DISCONTINUED TAKEOFF.

Source: SDR WRNA201510210001 · FAA SDRS
O · 2015-05-22 Matched by certificate designator
N950 · ATA 5313

DURING AIRCRAFT MAINTENANCE CHECK, INSPECTORS FOUND CORROSION IN THE CENTER CARGO COMPARTMENT BETWEEN BS 1641 & 1661 ON LONGERON 44R. REPAIRED IAW SRM 53-00-05, TYPE 1.

Source: SDR WRNA201506040004 · FAA SDRS
E · 2015-03-31 Matched by certificate designator
N902AR · ATA 7200

DURING DECENT THE NR 1 ENGINE, N2 VIBRATION PEAKED AT 4.5, 15,000 FEET, INDICATED AIRSPEED 300 KNOTS, FLIGHT IDLE POWER.

Source: SDR WRNA201504020004 · FAA SDRS
O · 2015-03-10 Matched by certificate designator
N955AR · ATA 2810

DURING ACFT MAINTENANCE CHECK INSPECTORS FOUND CORROSION ON TOP SURFACE OF UPPER AUXILIARY FUEL TANK BETWEEN STR 17 & 18 LT, STA 1199, LBL 108.

Source: SDR WRNA201503310003 · FAA SDRS
O · 2015-02-09 Matched by certificate designator
N955AR · ATA 2810

DURING ACFT MAINTENANCE CHECK, INSPECTORS FOUND CORROSION OTBD OF UPPER AUXILIARY FUEL TANK, FLOOR LT SIDE, BS 1239 TO 1255, LBL 109.

Source: SDR WRNA201503310002 · FAA SDRS
O · 2015-02-05 Matched by certificate designator
N955AR · ATA 2810

DURING ACFT MAINTENANCE CHECK INSPECTORS FOUND CORROSION ON SURFACE OF SURFACE AUXILIARY FUEL TANK BS 1219 TO 1229, RBL 68.

Source: SDR WRNA201503310001 · FAA SDRS
J · 2015-01-19 Matched by certificate designator
N903AR · ATA 3442

AFTER TAKEOFF ALL SYSTEMS WERE NORMAL. ONCE A RT TURN HEADING 120 DEGREES WAS INITIATED, THE CREW RECEIVED A "RADAR FAIL" MESSAGE WHILE IN THE TURN. AFTER A CLIMB OF 10,000 FT, THE CREW WAS UNSUCCESSFUL IN FIXING THE PROBLEM. AFTER DISCUSSING THE DUAL RADAR FAILURE WITH THE FLIGHT FOLLOWER THE CREW DECIDED TO RETURN TO DEPARTURE DUE TO NIGHT OPERATIONS AND WEATHER FORECASTED ALONG ROUTE AND AT DESTINATION. NO FUEL DUMP WAS REQUIRED. R & R WEATHER RADAR ANTENNA IAW AMM 34-34-03, OPS CHECK GOOD AND TEST PASSED.

Source: SDR WRNA20150029 · FAA SDRS
J · 2015-01-05 Matched by certificate designator
N902AR · ATA 2710

THE CREW REPORTED TAKEOFF WAS SMOOTH AND UNEVENTFUL. NOTICED AN OUT OF TRIM AND OPPOSITE RUDDER TRIM. RT INBD AILERON DEFLECTED TO FULL DOWN POSITION DURING FLIGHT AND WAS UNABLE TO ENGAGE AUTOPILOT. DIVERTED AND DUMPED APPROXIMATELY 25 MINUTES OF FUEL PERFORMED AN UNEVENTFUL LANDING. INBD AILIRON POWER CONTROL PACKAGE FOUND TO BE DAMAGED UPON VISUAL INSPECTION. R & R RT INBD AILERON POWER CONTROL ASSY.

Source: SDR WRNA201501080028 · FAA SDRS
O · 2014-12-08 Matched by certificate designator
N950AR · ATA 5330

DURING POSTFLIGHT WALKAROUND, FOUND A DENT ON FUSELAGE FWD OF THE FWD CARGO DOOR. REPAIRED IAW STS EO 100-2014-114. ALL WORK DOCUMENTED ON NR 26850, 002651, 003002.

Source: SDR WRNA20140027 · FAA SDRS
J · 2014-12-04 Matched by certificate designator
N901AR · ATA 2130

DURING CLIMB AT 9000 FT AGL, THERE WAS A CABIN ATTITUDE WARNING WITH AUDIO WARNING. PERFORMED QRH. PROCEEDED TO LEVEL OFF AT 14000' DUE TO TERRAIN. RETURNED TO AIRPORT. ALL CHECKLIST WERE COMPLETED. ACCOMPLISHED FIM 21-31, TASK 840, UNTIL STEP 3, PERFORMED CPCS GROUND TEST IAW AMM 21-31-00. SYSTEM OK.

Source: SDR WRNA201412080026 · FAA SDRS
N · 2014-10-14 Matched by certificate designator
N953AR · ATA 3150

THE CREW REPORTED THAT DURING TAKEOFF ROLL AT APPROXIMATELY 98KTS, THE MASTER WARNING LIGHT ILLUMINATED MOMENTARILY. ABORTED THE TAKEOFF. PERFORMED RTS OF DEU 1, DEU 2, AND DEU 3. RTS PASS IAW MM 31-61-02. OPS TEST OF MASTER WARNING ILLUMINATED PUSH BUTTON SWITCH. NO DISCREPANCIES NOTED.

Source: SDR WRNA201410160025 · FAA SDRS
J · 2014-10-13 Matched by certificate designator
N953AR · ATA 5100

THE CREW REPORTED THAT DURING TAKEOFF ROLL AT APPROXIMATELY 90KTS, THE MASTER WARNING LIGHT ILLUMINATED MOMENTARILY. AND THE AUTO BRAKES REACTED UNEVEN PULLING THE ACFT TO THE LT WITH A JERKING MOTION. CORRECTED THE SITUATION WITH MOVEMENT OF THE RUDDER AND NOSE WHEEL STEERING IN THE OPPOSITE DIRECTION. THE CREW PROCEEDED TO REJECT TAKEOFF. AS THE ACFT CAME NEAR TO A STOP, IT JOLTED ONCE AGAIN BUT THIS TIME HARDER THAN BEFORE. PROCEEDED TO TAXI TO THE GATE WITHOUT ANY FURTHER INCIDENT. PERFORMED RTS OF DEU 1, DEU 2, AND DEU 3. RTS PASS IAW MM 31-61-02. OPS TEST OF MASTER WARNING ILLUMINATED PUSH BUTTON SWITCH. NO DISCREPANCIES NOTED.

Source: SDR WRNA201410160024 · FAA SDRS
J · 2014-09-02 Matched by certificate designator
N950AR · ATA 3411

THE CREW REPORTED THAT DURING TAKEOFF, THERE WAS AN AIRSPEED DIFFERENCE AFTER 80KTS. THE F/O AIRSPEED INDICATOR DROPPED TO 55 KTS WHILE THE CAPTAIN’S AIRSPEED INDICATOR READ 95 KTS. REJECTED TAKEOFF AT 95 KIAS AND TAXIED BACK TO THE RAMP WITHOUT ANY FURTHER INCIDENT. FIM 34-11-02, PURGED LINES OF THE FIRST OFFICER’S PITOT SYSTEM IAW AMM 34-11-00. PERFORMED PITOT SYSTEM LEAK TEST IAW AMM 34-11-00. NO LEAKS NOTED.

Source: SDR WRNA201409040023 · FAA SDRS
N · 2014-09-01 Matched by certificate designator
N903AR · ATA 3297

THE CREW REPORTED THAT AFTER TAKEOFF, ATTEMPTED TO RAISE THE GEAR AND AN EICAS MESSAGE "GEAR TILT" DISPLAYED. FOLLOWED THE QRH PROCEDURES, LANDED WITHOUT ANY FURTHER INCIDENT. REPAIRED CHAFED WIRE AT LT WING LANDING GEAR JUNCTION BOX. OPS CHECKED NORMAL.

Source: SDR WRNA201409040022 · FAA SDRS
J · 2014-08-24 Matched by certificate designator
N953AR · ATA 2450

THE CREW REPORTED THAT PRIOR TO TOP OF DESCENT THAT A LEVEL 2 ALERT FOR GEN BUSS 3 FAULT WAS DISPLAYED IN THE EAD. FOLLOWED THE QRH PROCEDURES, DEPLOYED THE ADG AND NO FUEL DUMP WAS PERFORMED. LANDED WITHOUT FURTHER INCIDENT OR DELAY. PERFORMED FIM 24-20-17, STEPS 1-5, CHECKED T1-T3 FOR IDG TO GROUND. CHECKED CONNECTIONS P1-8559A & P1-8559B. CHECKED 53-393. GR-3 TO BTR-3, B7-7, B7-8 & B7-9 WITH GROUND = 250 OHMS. CHECKED GENERATOR RELAY & BUSS TIE RELAY. FOUND ALL NORMAL. FOUND RCCB B1-138 DIFFERENTIAL FAULT DEFECTIVE, R & R RCCB AND OPERATIONALLY CHECKED NORMAL.

Source: SDR WRNA201408280021 · FAA SDRS
J · 2014-08-21 Matched by certificate designator
N953AR · ATA 2497

THE CREW REPORTED DURING CRUISE FLIGHT, APPROXIMATELY 1 HOUR FROM DESTINATION THAT A LEVEL 2 ALERT FOR GEN BUSS 3 FAULT WAS DISPLAYED ON THE EAD. FOLLOWED THE QRH PROCEDURES, DEPLOYED THE ADG AND NO FUEL DUMP WAS PERFORMED. LANDED WITHOUT ANY FURTHER INCIDENT OR DELAY. REMOVED NR 3 BUSS ASSY FEEDER CABLES, NR 3 GR & NR 3 GEN CONTROL RCCB. STOWED ADG. OPS CHECK NORMAL. ACFT RELEASED FOR SERVICE.

Source: SDR WRNA201408260020 · FAA SDRS
J · 2014-08-20 Matched by certificate designator
N953AR · ATA 2410

THE CREW REPORTED DURING CRUISE FLIGHT, APPROX. 60 MILES FROM CARTAGENA VOR THAT A LEVEL 2 ALERT: GEN BUS 3 FAULT WAS DISPLAYED IN THE EAD. THE CREW THEREBY CONTACTED DISPATCH AND FLIGHT OPERATIONS. THE CREW FOLLOWED THE QRH PROCEDURES, DEPLOYED THE ADG AND NO FUEL DUMP WAS PERFORMED. THE CREW RETURNED WITHOUT ANY FURTHER INCIDENT OR DELAY. PERFORMED FUNCTIONAL TEST OF THE GEN BUSS FAULT RESET IAW 24-21-00.ENGINE RUN WAS PERFORMED IAW 71-00-00. EPCU RTS TEST PASSED.

Source: SDR WRNA201408260019 · FAA SDRS
J · 2014-08-19 Matched by certificate designator
N953AR · ATA 2410

THE CREW REPORTED THAT DURING CRUISE FLIGHT, APPROXIMATELY 50 MINUTES AFTER TAKEOFF, A LEVEL 2 ALERT OF A GENERATOR BUSS 3 FAULT WAS DISPLAYED IN THE EAD. FOLLOWED QRH PROCEDURES, DEPLOYED THE ADG AND NO FUEL DUMP WAS PERFORMED. RETURNED TO DEPARTURE WITHOUT FURTHER INCIDENT. R & R DIFFERENTIAL PROTECTION CURRENT TRANSFORMERS, T1-9071, T1-9074 & T1- 9080. GROUND OPS NORMAL. SYSTEM CHECKED OK.

Source: SDR WRNA201408200018 · FAA SDRS
O · 2014-08-13 Matched by certificate designator
N951AR · ATA 2810

DURING ACFT HEAVY MAINTENANCE CHECK, INSPECTORS FOUND EXFOLIATION CORROSION ON UPPER SURFACE OF THE CENTER AUXILIARY FUEL TANK, STATION 1239.

Source: SDR WRNA201403310028 · FAA SDRS
J · 2014-07-25 Matched by certificate designator
N953AR · ATA 7830

CREW REPORTED THAT DURING TAKEOFF, THRUST REVERSER UNLOCK LIGHT ILLUMINATED LESS THAN 80 KNOTS. CREW RETURNED TO THE GATE IAW MAINTENANCE PROCEDURE TO LOCK OUT THRUST REVERSER. CREW ATTEMPTED ANOTHER TAKEOFF AND THE SAME OCCURRENCE OF THE THRUST REVERSER UNLOCK LIGHT INDICATION ILLUMINATED AGAIN LESS THAN 80 KNOTS CAUSING A SECOND REJECTED TAKEOFF. CREW RETURNED TO THE RAMP WITHOUT ANY FURTHER INCIDENT.

Source: SDR WRNA20140016 · FAA SDRS
J · 2014-07-21 Matched by certificate designator
N950AR · ATA 7200

ON REACHING TOP OF CLIMB, A LEVEL 2 OIL PRESSURE LOW DISPLAYED. CREW FOLLOWED THE QRH PROCEDURES SIMULTANEOUSLY FOLLOWING THE QRH PROCEDURES "ENGINE SHUTDOWN IN FLIGHT" FOR ENG NR 2. THE CREW ACCOMPLISHED THE CHECKLIST THEN PROCEEDED TO DUMP APPROXIMATELY 50 KGS OF FUEL. THE CREW DECLARED AN EMERGENCY LANDING, BUT RETURNED BACK TO DEPARTURE WITHOUT ANY FURTHER INCIDENTS OR DELAYS. VISUALLY INSPECTED ENG NR 2, FOUND METAL SEDIMENT AT CHIP DETECTORS AND IN MAIN OIL FILTER. REPLACED NR 2 ENGINE.

Source: SDR WRNA201407230015 · FAA SDRS
O · 2014-06-26 Matched by certificate designator
N950AR · ATA 5730

DURING HEAVY CHECK, LT WING UPPER PLATE AT LWS 160 AND S15L WAS FOUND TO BE CORRODED. DAMAGE REPAIRED IAW EO SLC-140317.

Source: SDR WRNA20140011 · FAA SDRS
O · 2014-06-26 Matched by certificate designator
N950AR · ATA 5320

DURING HEAVY MAINTENANCE, MAINTENANCE FOUND UPPER PLATING AROUND BS 1229 BETWEEN RBL 57 TO 78 CORRODED. REPAIRED IAW EO SLC-140609.

Source: SDR WRNA201406260009 · FAA SDRS
O · 2014-06-26 Matched by certificate designator
N950AR · ATA 5320

DURING HEAVY CHECK, UPPER PLATING AROUND BS 1229 AROUND RBL 8 FOUND CORRODED. REPAIRED IAW EO SLC-140611.

Source: SDR WRNA201406260010 · FAA SDRS
O · 2014-06-26 Matched by certificate designator
N950AR · ATA 5321

DURING HEAVY CHECK, FLIGHT COMPARTMENT, MAIN DECK, AND LOWER CARGO COMPARTMENT FLOOR PANELS WERE FOUND DAMAGED. REPAIRED FLOOR PANELS IAW EO SLC-140313.

Source: SDR WRNA201406260012 · FAA SDRS
O · 2014-06-26 Matched by certificate designator
N950AR · ATA 2550

DURING HEAVY CHECK, MAIN DECK CARGO HANDLING SYSTEM, CENTERLINE RESTRAINT ASSY SIDE FITTINGS WERE FOUND CRACKED. R & R 38 EACH CENTERLINE RESTRAINTS SIDE FITTINGS. REPAIR OF SIDE FITTINGS ACCOMPLISHED IAW EO SLC-121214.

Source: SDR WRNA201406260013 · FAA SDRS
C P · 2014-06-25 Matched by certificate designator
N955AR · ATA 3411

DURING TAKEOFF, AIRCRAFT SPEED SCALE AND GREEN ACCELERATION LINE WERE NOT PRESENT ON EITHER THE CAPTAIN OR F/O PFD'S, NO AIRSPEED INDICATION. INSTEAD "TAXI" WAS STILL DISPLAYED. THE CREW MADE THE DECISION TO ABORT TAKEOFF APPROXIMATELY BETWEEN 85-90 KTS. FOLLOWED POST FLIGHT AND TAXI PROCEDURES BACK TO THE GATE WITHOUT ANY OTHER FURTHER INCIDENT. FOUND INSECTS IN PITOT TUBES. PURGED PITOT STATIC SYS IAW AMM 24-11-00. 2. R & R STATIC RIGID LINE AT RT STATIC PORT IAW AMM 20-50-01.

Source: SDR WRNA201406260014 · FAA SDRS
N · 2014-06-11 Matched by certificate designator
N955AR · ATA 5270

DURING CLIMB THROUGH 10,000 FT, A LEVEL 2 ,CARGO DOOR FWD A ALERT DISPLAYED. FOLLOWED QRH PROCEDURES AND ACCOMPLISHED CHECKLIST. RETURNED TO DEPARTURE WITHOUT ANY FURTHER INCIDENTS. VISUALLY INSPECTED CARGO DOOR, FOUND CARGO DOOR CLOSED AND LOCKED.

Source: SDR WRNA20140612008 · FAA SDRS
E J · 2014-05-22 Matched by certificate designator
N953AR · ATA 3244

DURING TAKEOFF ROLL, PRIOR TO V1, CREW REPORTED THEY FELT VIBRATION AND SIMULTANEOUSLY "LEVEL 2 ALERT" INDICATED "TIRE FAILURE," NR 1 TIRE FAIL DISPLAYED. THE CREW ABORTED TAKEOFF IAW PROCEDURE. ALSO, DUE TO THE HIGH-ENERGY STOP, THIS CAUSED AN OVER TEMP OF THE THERMAL PLUGS IN 4 OTHER TIRES.

Source: SDR WRNA201405230007 · FAA SDRS
J · 2014-05-11 Matched by certificate designator
N953AR · ATA 2421

DURING CRUISE, AT APPROXIMATELY 100NM SOUTH OF AIRPORT, LEVEL 2, GEN 3 BUSS FAIL ALERTED. CREW FOLLOWED THE QRH PROCEDURES, DEPLOYED THE ADG. CONTINUED FLIGHT AS PLANNED AND LANDED AT FLIGHT DESTINATION WITHOUT ANY FURTHER INCIDENTS. PERFORMED ENGINE RUN. PERFORMED FUNCTIONAL TEST OF THE GENERATOR BUSS FAULT TEST IAW AMM-24-21-00. STOWED ADG IAW AMM-24-21-00. OPS CHECKED NORMAL.

Source: SDR WRNA20140513006 · FAA SDRS
M J · 2014-04-24 Matched by certificate designator
N955AR · ATA 3240

CREW REPORTED DURING TAKEOFF ROLL, ONE OR MORE OF THE BRAKES WERE GRABBING AT APPROXIMATELY 80 KNOTS ON THE LT SIDE. ACFT ACCELERATION THEREBY SLOWED DOWN. THE CREW PROCEEDED BY REJECTING TAKEOFF AND RETURNED TO THE RAMP WITHOUT FURTHER INCIDENT. FOUND NR 10 BRAKE INOPERATIVE. DEACTIVATED BRAKE.

Source: SDR WRNA20140005 · FAA SDRS
J · 2014-03-29 Matched by certificate designator
N953AR · ATA 2421

CREW REPORTED THEY LOST THE RT EMERGENCY AC BUSS. THE ALERT WAS GENERATOR BUSS 3 FAULT. HAD ONLY A SINGLE GENERATOR OPERATIVE. FOLLOWED QRH PROCEDURES, DEPLOYED ADG AND LANDED WITHOUT FURTHER INCIDENT. PERFORMED TASK IAW FIM 24-20-05. AUTO RESET OF EPCU. STOWED ADG. OPS CHECKED NORMAL.

Source: SDR WRNA201404010004 · FAA SDRS
J · 2014-01-25 Matched by certificate designator
N955AR · ATA 7200

DURING TAKEOFF ROLL, CREW RECEIVED A LEVEL 2 ALERT ON THE EAD WITH A MASTER CAUTION LIGHT FOR ENGINE N1, RPM HIGH. DISCONTINUED TAKEOFF. MAXIMUM N1 RPM RECORDED WAS 111.6. NO FURTHER INCIDENT. FOLLOWED PROCEDURES IN FIM 77-11-06, INSPECTED ENGINE. NO FAULTS NOTED. REPLACED EEC IAW AMM 71-02-07 & AMM 71-02-06, RAN NR 2 ENGINE. OP CHECKED GOOD AND ACFT RETURNED TO SERVICE.

Source: SDR WRNA201301310002 · FAA SDRS
R Y J · 2014-01-21 Matched by certificate designator
N952AR · ATA 7200

DURING TAKEOFF ROLL, CREW DISCOVERED THE ACFT SUFFERED AN AUDIBLE ENGINE STALL AND FAILURE. CREW ABORTED TAKEOFF AND RETURNED TO GATE WITH NO FURTHER INCIDENT. MX DISCOVERED METAL IN THE EXHAUST OF THE ENGINE, WITH LOTS OF METAL ON RUNWAY AS WELL. REMOVED AND REPLACED NR 3 ENGINE.

Source: SDR WRNA201301270017 · FAA SDRS

Linked aircraft

No aircraft currently linked.